Deployment NameGliderProjectDeployedRecoveredDaysDistancePayload BayOSNotes
bios_anna-20170220T1757bios_annaBIOS2017-02-20
17:57Z
2017-07-05
16:25Z
134.9649.9 km91367.20

All Notes (20)

Created by: dkaragon @ 2017-08-15 09:40:24Informational

Digifin error

Initial m_fin was -.49

Tried to increase fin limits and move fin beyond above and inside above. Fin still wont move. Setnumwarn increased to do this. Spin rate appears to be 30 deg/min CC which agrees with negative fin but seems a bit slow.


Also have this error to deal with on no fin missions or out of service when transferring data

g_shell_mission_execute():Some device(s) went OUT OF SERVICE during CmdDispatch()
23957 ERROR behavior surface_4: process_user_keystrokes(): Fatal device error from g_shell_mission_execute()

23957 ERROR behavior surface_4: bs_waiting_control_c(): process_user_keystrokes() caused mission abort
23957 behavior surface_4: SUBSTATE 7 ->-1 ERROR: per process_user_keystrokes(), probably a device error
23957 behavior surface_4: STATE Active -> ERROR
23957 ERROR behavior surface_4: Entered B_ERROR State
23957 ERROR behavior ?_-1: layered_control(): The surface behavior entered B_ERROR state.
23963 ERROR behavior ?_-1: abort_the_mission(0): (6)MS_ABORT_BEH_ERROR

Created by: dkaragon @ 2017-07-12 11:40:39Informational

CTD 9136
FLBBCD 3409
Optode 279

Created by: dkaragon @ 2017-07-05 13:55:05Informational

Recovered by AE

Created by: administrator @ 2017-07-01 09:36:26Informational

Begin diurnal experiment
Dives to 500 m, double yos
sampling on dives and climbs

Created by: administrator @ 2017-07-01 09:35:34Informational

29Jun -> 1Jul Diving in tandem with Jack for sensor comparison

Created by: administrator @ 2017-06-04 09:30:16Informational

dives to 920; double yos; 8 hour no comms

Created by: dkaragon @ 2017-06-02 21:51:06Informational

Fin came online after setnumwarn and use + digifin.

Set GliderDos N -1 >get x_fin_deadband
= 0.040000 rad

GliderDos N -1 >get x_fin_max
= 0.220000 rad

And set .24 to longterm.sta for f_fin_deadzone_width

Roughly 15 deg of fin, set deadband back to .04

Created by: dkaragon @ 2017-06-02 11:36:58Informational

Digifin error

Initial m_fin was -.49

Tried to increase fin limits and move fin beyond above and inside above. Fin still wont move. Setnumwarn increased to do this. Spin rate appears to be 30 deg/min CC which agrees with negative fin but seems a bit slow.


Also have this error to deal with on no fin missions or out of service when transferring data

g_shell_mission_execute():Some device(s) went OUT OF SERVICE during CmdDispatch()
23957 ERROR behavior surface_4: process_user_keystrokes(): Fatal device error from g_shell_mission_execute()

23957 ERROR behavior surface_4: bs_waiting_control_c(): process_user_keystrokes() caused mission abort
23957 behavior surface_4: SUBSTATE 7 ->-1 ERROR: per process_user_keystrokes(), probably a device error
23957 behavior surface_4: STATE Active -> ERROR
23957 ERROR behavior surface_4: Entered B_ERROR State
23957 ERROR behavior ?_-1: layered_control(): The surface behavior entered B_ERROR state.
23963 ERROR behavior ?_-1: abort_the_mission(0): (6)MS_ABORT_BEH_ERROR

Created by: administrator @ 2017-05-12 02:17:31Informational

Reduced pump throw to -180 / +160

Created by: administrator @ 2017-05-09 05:47:31Informational

Pump throw -200 / +180

Created by: administrator @ 2017-05-08 12:45:39Informational

Six wing rail weights removed by R/V AE / small boat.

Created by: administrator @ 2017-05-08 05:59:41Informational

200 m dives, full pump throw.
Waiting for AE to rendezvous and remove rail weights

Created by: administrator @ 2017-05-01 11:08:49Informational

Added 20cc to pump on climbs.
Pump throw now -130/+230. Will schedule a recovery and remove 50g when AE visits Hydrostation.

Created by: dkaragon @ 2017-04-17 11:32:33Informational

Pump oil passive retraction started on this mission, perhaps slightly on last mission after reading notes.

Roughly 7k tot num inflections

Created by: administrator @ 2017-03-25 07:48:03Informational

Experienced bug (same day as other 2 gliders)
DRIVER_ODDITY:science_super:906:Input ringbuf overflow

Fixed by cycling power on science side
put c_science_on 0
put c_science_on 1

Created by: administrator @ 2017-03-19 11:04:59Informational

put u_alt_min_depth 1500
put u_low_power_cycle_time 30

sent all *sbd (there was a backlog -- Fast Script TBDSBD not giving enough time at surface for sending logs-??)

goto file set to 0.5 km box at Hydro

Created by: administrator @ 2017-03-19 11:04:56Informational

pump throw -130 / +210
changed initial waypt to -1 (first after last)
sci sampling on dives only

Created by: administrator @ 2017-03-19 11:04:52Informational

pump throw -130 / +210
sci sampling on dives only
initial waypoint -1 (first after last, in goto)

Created by: dkaragon @ 2017-03-19 11:04:46Informational

Deployed by R/V Endeavor at Hydrostation S
software version 7.20
CTD 9136
FLBBCD 3409
Optode 279

Created by: dkaragon @ 2017-03-19 11:04:42Informational

test