Deployment NameGliderProjectDeployedRecoveredDaysDistancePayload BayOSNotes
ru21-20100722T1631ru21eline2010-07-22
16:31Z
2010-08-03
15:45Z
12.0182.9 km00006.37

All Notes (7)

Created by: dkaragon @ 2010-07-30 14:36:43Informational

duty cycling the ADCP sensor to save some power over the weekend. Will turn it back on full time when we get closer to recovery.

Created by: kerfoot @ 2010-07-29 10:33:56Informational

Science Payload:

pumped CTD
ADCP

first ADCP payload

Configured with software version 7.2

Created by: kerfoot @ 2010-07-27 16:46:52Informational

Email from David Aragon:

Webb,

I just wanted to shoot this email out while we have a glider flying 7.2 with pumped CTD and ADCP. I may not get around to entirely troubleshooting on the glider out there, perhaps better chance of doing so in lab in simulation.

50% of the time we re-task and issue a ctrl^f, the glider aborts for no_input.

We are running with c_science_send_all which could be adding to the problem since it seems \'overload\' related? However at the surface I am
not sure much data is going across the clothesline. If I see any more of this on any other glider or have more I will follow up.

Thanks.

David K. Aragon

Created by: dkaragon @ 2010-07-26 22:08:57Informational

!put u_dvl_es_expected_salinity 31

Created by: dkaragon @ 2010-07-26 14:11:32Informational

Hopefully recovering this Friday.

Doing steering tests.

Glider doesn\'t appear like it lost a wing, but still too heavy. Water is pretty light out there, 1018\'ish

Turned ADCP on at surface now, battery usage should increase. Flying by battpos so bettery pitch angles.

Created by: dkaragon @ 2010-07-23 22:28:04Informational

another ctrl^f no input abort

Something for Webb to see, back on missions.

Created by: dkaragon @ 2010-07-23 11:44:40Informational

Tuning, zero\'ed ocean pressure