All Notes (11)
AZFP back to every downcast, CTD back to every yo, pH/Optics back to every 3rd
2 days ago all sampling to 100th yo, just to save power since we got washed back during storm.
AZFP to -3 sampling until we recover route.
pH sampling to -3 nth yo
Optics flbbcd sampling -3, everything else full duty, AZFP downs only
Rosette problems on shallow #2, Niskin used before shallow #3. Shallow 2 or 3 good for comparison
AZFP params
Parameters - 2025 02 26 18:07:11.09
Deployment Parameters
Number of boards... 3
Board 0 BoardFreq. 38
Board 1 BoardFreq. 120
Board 2 BoardFreq. 200
SoundSpeed .... 1500.00
Output ............ FLASH
ACQ Start Date .... 2025 2 14 18 53 34
NumPhases ......... 1
P01 Start Date .... 2025 2 14 18 53 34
P01 Duration(days). 300.0000
P01 Phase Type........ Normal
P01 PingPeriod ....... 1
P01 BurstInterval..... 2
P01 PingsPerBurst..... 1
P01 AverageBurstPings. 0
P01 F1 BoardFrequency.. 38
P01 F1 acquire......... 1
P01 F1 PulseLen ....... 500
P01 F1 DigRate (hz).... 40000
P01 F1 RangeSamples.... 5300
P01 F1 LockOutIndex.... 0
P01 F1 RangeAvgSamples. 53
P01 F1 StorageFormat... linear
P01 F2 BoardFrequency.. 120
P01 F2 acquire......... 1
P01 F2 PulseLen ....... 500
P01 F2 DigRate (hz).... 40000
P01 F2 RangeSamples.... 5300
P01 F2 LockOutIndex.... 0
P01 F2 RangeAvgSamples. 53
P01 F2 StorageFormat... linear
P01 F3 BoardFrequency.. 200
P01 F3 acquire......... 1
P01 F3 PulseLen ....... 500
P01 F3 DigRate (hz).... 40000
P01 F3 RangeSamples.... 5300
P01 F3 LockOutIndex.... 0
P01 F3 RangeAvgSamples. 53
P01 F3 StorageFormat... linear
load_mission(): Opening Mission file: ru39.mi
Setting SENSOR u_abort_min_burn_time(sec) value 600.000000
Setting SENSOR u_abort_max_burn_time(sec) value 64800.000000
Setting SENSOR u_reqd_depth_at_surface(m) value 2.000000
Setting SENSOR u_hd_fin_ap_run_time(secs) value -1.000000
Setting SENSOR u_hd_fin_ap_gain(1/rad) value 1.500000
Setting SENSOR u_hd_fin_ap_igain(1/rad-sec) value 0.015000
Setting SENSOR u_hd_fin_ap_dgain(sec/rad) value 8.000000
Setting SENSOR u_hd_fin_ap_hardover_holdoff(sec) value 30.000000
Setting SENSOR u_pitch_ap_gain(1/rad) value -2.000000
Setting SENSOR u_pitch_ap_dgain(s/rad) value -1.000000
Setting SENSOR u_pitch_ap_deadband(rad) value 0.060000
Setting SENSOR u_min_pitch_ap_period(sec) value 2.000000
Setting SENSOR u_max_pitch_ap_period(sec) value 60.000000
Slightly too stable?
Operating System: 10.08
Instruments:
Seabird Slocum Glider CTD
9917
9/6/2024
Seabird pH
12110
6/11/2024
Wetlabs FLBBCD-SLC
7788
9/8/2022
ASL AZFP (fish configured)
59025
4/12/2024
38,120,200 kHz
Vemco VMT
1564554 ID51593 no cal date
Strap-on, no data flow through glider
Deployed by Nicole Waite, Jess Leonard, Delphine Mossman, and Lauren Cook aboard TowBoat out of Manasquan, NJ with shoreside support from David Aragon.
Water sampling with single niskin at 2m, 8m, 15m. Rosette CTD had issues and other cage CTD did not work either. No comparison CTD cast.