All Notes (15)
Rx-Live worked in the lab after recovery. Manipulating the cable didn't cause it to break either.
Inside the science bay the connector going to the board was not seated completely - this has been fixed.
tail stem bent to starboard slightly - this might be the cause of the heavy negative fin. vemco cables also slightly on the starboard side.
repositioned vemco cables for next Invenergy mission towards port side and intentionally cocked fin to port.
science warnings occurred during file transfers/drops.
recovered by Jess Leonard, Chip Haldeman, and deckhand on RV Rutgers out of Tuckerton, NJ
Science off, thruster on.
Dive GPS
2024-02-16T20:02:02Z
BAD GPS position !
Take a look at the science odd/warn after mission
13 science_super I u 3 20 5 0 [ 0 0 0] [ 1 1 0] [ 26 19 0]
Every +14th for CTD, Optode, FLBBCD (try to listen a little more) Right whales in area.
Heavy negative fin, may be a reoccurring problem, fix for next mission.
Investigate previous bottom samples.
Trying short missions without altimeter filter
Setting SENSOR u_abort_max_burn_time(sec) value 64800.000000
Setting SENSOR u_reqd_depth_at_surface(m) value 2.250000
Setting SENSOR u_hd_fin_ap_run_time(secs) value 12.000000
Setting SENSOR u_hd_fin_ap_gain(1/rad) value 1.500000
Setting SENSOR u_hd_fin_ap_igain(1/rad-sec) value 0.015000
Setting SENSOR u_hd_fin_ap_dgain(sec/rad) value 8.000000
Setting SENSOR u_hd_fin_ap_hardover_holdoff(sec) value 30.000000
Setting SENSOR u_min_altimeter(m) value 4.500000
Setting SENSOR u_max_altimeter(m) value 25.000000
Setting SENSOR u_alt_reqd_good_in_a_row(nodim) value 3.000000
Setting SENSOR u_alt_filter_enabled(bool) value 0.000000
Setting SENSOR m_altitude_rate(m/s) value -1.000000
Setting SENSOR u_pitch_ap_gain(1/rad) value -1.000000
Setting SENSOR u_pitch_ap_dgain(s/rad) value -1.000000
Setting SENSOR u_pitch_ap_deadband(rad) value 0.069000
Setting SENSOR u_min_pitch_ap_period(sec) value 30.000000
Setting SENSOR u_max_pitch_ap_period(sec) value 60.000000
ATTEMPT 2 ON RXLIVE = NO COMMS Still turned off
VR2C Rx Live turned off until able to troubleshoot again
VEMCO doesn't appear to be working. .cfg seems to be OK as well as mission and MA, tried to talk to it via uart but didn't succeed.
No .vem since transferring glider to SBU last Wed 1/17/24
robots4whales http://robots4whales.whoi.edu/rutgers0124/rutgers0124_maracoos_02.shtml
Deployed by Charles Flagg, Mate Bryan Waag, and Capt Jim Reynolds aboard TowBoatUS south of Fire Island Inlet.
Operating System: 10.08
Seabird pumped CTD
9646
6/29/2021
Wetlabs FLBBCD-SLC
6312
6/17/2020
Aanderaa Optoxe Oxy4831
893
7/25/2023
In-house check: 12/20/2023
WHOI DMON
3A231D06
Head s/n 111
Vemco RxLive
457001