All Notes (54)
Dataset workup:
Have all dbds & ebds (01420000-01770016) from beginning of deployment until glider was picked up on 2011-11-16, just N of the Azores. After that,data is very spotty.
Glider recovered due to low battery voltage. Redeployment to be determined.
two yo\'s to 980m initiated - new waypoint
!put u_alt_min_depth 1100
!put u_use_current_correction 0
too much to probably summarize here...will leave it at that we are underway again.
diving to 980
!put u_alt_min_depth 500
Turned off science to get an idea of change in energy consumption:
use - science_super
Turned off full drive, making decent progress.
New yo file, still 4 yos to 300m.
put c_climb_bpump 212.5
put c_dive_bpump -87.5
Turned on full drive (still diving to 300m):
!put c_dive_bpump -1000
!put c_climb_bpump 1000
new yo file
After leak abort at 650m (2011-11-08T16:34:59), we kept glider at surface.
At 2011-11-08T21:30:00, run leif.mi:
changed yo depth to 300m
set c_leakdetect_time 0
loadmission waterclr.mi
Silbo aborted around 07:00 EST for a leak detect in the aft compartment.
ABORT HISTORY: total since reset: 18
ABORT HISTORY: last abort cause: MS_ABORT_LEAK
ABORT HISTORY: last abort details: There is a leak in the aft compartment.
ABORT HISTORY: last abort time: 2011-11-05T10:17:30
ABORT HISTORY: last abort segment: silbo-2011-305-0-19 (0169.0019)
ABORT HISTORY: last abort mission: LEIF.MI
At 940m on the second dive of segment 2011-305-0-19, the aft end leak detector detected a leak. A leak is defined as voltage lower than 2.0 V.
The data resolution was infrequent for this sensor (~60 secs). We were able to see from data a low voltage reading (~1.2 V) around the time of the abort. There were no other readings < 2.0 V as the glider
surfaced, however, in the surface dialog we saw the following sensor value:
sensor:m_leakdetect_voltage(volts)=1.15299145299145 54.152 secs ago
By the time I was able to get to the glider, the leakdetect voltage was back above 2.5
It is possible then that no other low voltages were recorded due to the low recording frequency for this sensor, or another anomaly.
##Actions taken:
17:30 EST
Running a single yo to 30m with the following configuration:
Added sensors to the SBD/MBD lists:
m_leakdetect_voltage
m_leakdetect_voltage_forward
m_battery_inst
m_vacuum
put c_leakdetect_time 0 (was 60)
New leif.mi mission, with overtime = 7200
New yo10.ma, single yo to 30m.
2011-Nov-03
Deleted a number of files to clear up space.
!del C:\\sentlogs\\*.*
!del C:\\logs\\0162001*.dbd/mlg
!del C:\\logs\\0163001*.dbd/mlg
!del C:\\logs\\0164001*.dbd/mlg
2011-Nov-04
Deleted the following files:
!del C:\\logs\\0155001*.dbd/mlg
!del C:\\logs\\0155003*.dbd/mlg
!del C:\\logs\\0155005*.dbd/mlg
!del C:\\logs\\0155007*.dbd/mlg
!del C:\\logs\\0152001*.dbd/mlg
!del C:\\logs\\0152003*.dbd/mlg
!del C:\\logs\\0152005*.dbd/mlg
!del C:\\logs\\0151001*.dbd/mlg
!del C:\\logs\\0151003*.dbd/mlg
!del C:\\logs\\0149001*.dbd/mlg
!del C:\\logs\\0148001*.dbd/mlg
!del C:\\logs\\0148003*.dbd/mlg
!del C:\\logs\\0148005*.dbd/mlg
!del C:\\logs\\0148007*.dbd/mlg
!del C:\\logs\\0148009*.dbd/mlg
!del C:\\logs\\0148011*.dbd/mlg
cycled air pump solenoid several times
Glider aborted due to MS_NOINPUT()
New yo (single yo) and new waypoint
Modified leif.mi, removing u_use_current_correction sensor (was = 0).
sequence leif.mi(5)
put u_use_current_correction 1
Changed climb target depth to 25m
New sbdlist and mbdlist (in archive)
New yo file:
c_target_depth(m) 200
d_speed_min(m/s) 0.04
c_speed_min(m/s) -0.04
!put u_alt_min_depth 1000
--------------------------------
861281 27 sensor: u_alt_min_depth = 1000 m
Changed:
676927 85 sensor: u_alt_min_depth = 450 m
new waypoints
-2643.883 3843.565
-1708.000 3303.500
Changed back to reduced drive.
put c_climb_bpump 1000
put c_dive_bpump -1000
new yo file read with appropriate battpos
New waypoints:
-2200.000 3900.000
-1708.000 3303.500
Changed c_iridium_no_char_timeout from 11 minutes to 15 minutes.
Cycled solenoid several times (c_air_pump -1, 1 ) to help with air pump
sequence leif.mi(5)
New waypoints:
-2700.000 3900.000
-1708.000 3303.500
Aborted for deadman last night, 9/16,17
This morning aborted for iridium
Looks like script might not be set correctly? Or that it just sat at surface with no commands to it.
file xfer and callback 5 performed, will let it autosequence in case someone wants to grab it.
cycled solenoid a few times.
new waypoints:
-2200.000 3900.000
-1708.000 3303.500
Imagery processing back up
Glider aborted due to Iridium timeout error. This appears to have been due to the Dockserver XML script, not the glider. Downloaded files and resequenced leif 4 times.
New waypoint:
-2655.000 3748.000
-1708.000 3303.500
New yo file in to-glider:
dive battpos = 0.4, climb = 0.05
Reduced the minimum vertical speed to +/- 0.04 m/s
2011-09-01 09:00 lcooney
silbo-2011-236-0-40: Changed to using full drive and pitch servo, only performing one yo. On next surfacing, will calculate the avg battpos, and go back to 2 yos and constant battpos. The following commands were sent:
!sbd + m_battpos
!put c_climb_bpump 1000
!put c_dive_bpump -1000
2011-09-01 13:20 EST lcooney
silbo-2011-236-0-42: After examining the battpos from the previous yo w/ servo, commanded back to 2 yos with full drive, battpos = 0.06 for dive, 0.194 for climb.
2011-09-01 20:19 EST lcooney
after 2 yos, changed back to using the partial drive, and old yo file with 0.1 inch battpos is saved in archive, 20110902T001448_yo10.ma
!put c_climb_bpump 212.5
!put c_dive_bpump -87.5
Changed the following at 8-25-11 13:45 surface:
new waypoints:
-2455.000 3748.000
-1708.000 3303.500
increase from 300 to 600 wait for gps time on pitch not command surface
changed the pitch battery placement by .1 inch for dive and climb to result in shallower dive and climb angles
cycled solenoid a number of times
sequence mission 5 times
at 16:18 surfacing changed max time in gliderdos to 60 seconds and opened and closed the solenoid valve a number of times. air bladder did begin inflating during this period.
ABORT HISTORY: total since reset: 6
ABORT HISTORY: last abort cause:
deadman abort tracking:
MS_ABORT_DEVICE_ERROR ABORT HISTORY: last abort details: The deadman device driver returned an error.
ABORT HISTORY: last abort time: 2011-08-13T19:22:48 ABORT HISTORY: last abort segment: silbo-2011-216-0-60 (0151.0060) ABORT HISTORY: last abort mission: LEIF.MI
new waypoints:
-1900.000 5030.000
-2455.000 3748.000
-1708.000 3303.500
Note primarily for tracking of deadman aborts -
this mlg was not pulled:
ABORT HISTORY: last abort cause: MS_ABORT_DEVICE_ERROR
ABORT HISTORY: last abort details: The deadman device driver returned an error.
ABORT HISTORY: last abort time: 2011-08-05T02:13:14
ABORT HISTORY: last abort segment: silbo-2011-211-1-31 (0150.0031)
Email from Ben Allsup - 2011-07-30:
update - Logs pulled at 14:56 surfacing. Sent back to primary number
Silbo aborted… Got home and got my computer started just in time to see the dive… It appears it was a deep pump movement error we have been addressing in programming a controller pic chip and will make a software adjustment as well in the near future.
May pull a log at next opportunity
Ben
New yo file in to-glider directory. Changed d_pitch_value from 0.4 to 0.5 (dive pitch angle has been shallow lately).
c_speed_min(m/s) from -0.08 to -0.17
Also changed waypoints to:
-2300.000 4943.711
-1708.000 3303.500
2011-07-08 23:00 EST
Changed c_speed_min(m/s) from -0.17 to -0.15 (was hitting -0.17 too early in the climb)
2011-07-09 09:55 EST
Changed c_speed_min from -0.15 back to -0.17, and commanded c_depth_rate_avg_num 40. Hopefully this will cause speed control to kick in later.
stopped mission and restarted sequenced 3 times. current correction off again.
TWRC Firewall issues preventing silbo from updating at marine.rutgers.edu (glider was connecting to dockserver ok) (7/2/2011 @ 11:39pm):
Hello,
TWR is having firewall trouble... Silbo flying well and not overdue. More tomorrow about moving waypoints.
Ben
!put u_use_current_correction 1
!put u_alt_min_depth 1000
Printed warning dialog to log
the following waypoints are waiting for the next surfacing:
-2405.000 6225.000
-2204.230 6305.536
heading south west of present location to hopefully find less or southerly current indicated by HYCOM data
Stopped leif.mi
Uploaded new sbdlist and mbdlist (in archive directory as 20110627T194022XXX)
Restarted leif.mi
stop mission edited:
sensor: u_alt_min_depth(m) 750
changed mafile for 4 half yo\'s (2 deep dives)
increased no comms surface to 8.5 hours
restarted mission sequenced 3 times
!put u_alt_min_depth to 325 at 16:14 surface
I have been running numbers at each surfacing to compare the most recent leg against the rest of the journey. This comparison uses a direct path to the Canaries and also assumes that we can apply the last segment data to the remainder (both poor assumptions). So with that said here are the most recent results:
segment speed kh 1.243620607
total hrs remain at segment usage 3140.025165
remaining coulomb amp/hrs 700.0713744
coulomb amphr needed at segment rate -470.1823208
days required at segment speed 130.8343819
days of energy available at present c/d -194.8040185
total reserve energy base on last segment usage% 32.8379451
That said the glider is flying into pretty unfavorable currents at the moment if this were to continue and we use the same calculations and instead of using distance over segment we use distance made good towards Canaries over the same segment the results look much worse (path planning will be come critical this week):
segment speed kh 0.487481945
total hrs remain at segment usage 8010.553086
remaining coulomb amp/hrs 700.0713744
coulomb amphr needed at segment rate -1199.487343
days required at segment speed 333.7730453
days of energy available at present c/d -194.8040185
total reserve energy base on last segment usage% -71.3378645
Autoballast completed. Running glider with:
- 6 half yos
- dive ballast=-87.5, climb=212.5.
- dive battpos=0.4, climb = -0.05 (may need to tune these.)
New file in archive: 20110625T060332_yo10.ma
As well, changed the altimeter depth u_alt_min_depth to 225
Began Autoballast routine. Vehicle should now be surfacing after 2 half-yos.
-Ended leif.mi.
-Uploaded new config.srf, mbdlist.dat, reduced sbdlist.dat,reinitab.mi (to reinitalize Autoballast) and new Autoballast yo10.ma (all in archive: 20110624T185233_...)
-Changed f_battpos_deadzone_width from 0.2 to 0.1 (can consider changing this back...but if we are going to consistently use const battpos, then it\'s not an issue.)
-Running leif.mi again, with Autoballast enabled.
TWR network was down over night (23Jun2011 19:24 EST - 24Jun2011 09:24 EST). Both rudics and modem were unreachable. Glider called in over alternate number. Sent the command to call back over primary (c_iridium_current_num 0). Sent all tbd files, but only most recent sbd (silbo-2011-173-5-16.sbd) was sent. SBD\'s gathered during the down time (173-5-11 thru 173-5-15) were manually moved to the sentlogs directory.
Glider is now on its way with revised leif.mi and gotol10 (in archive)
From: ben allsup [ballsup@webbresearch.com]
Sent: Thursday, June 23, 2011 11:41 AM
To: silbo-crossing@plocan.eu
Subject: Silbo in the news and update
Hello all,
6 of 4000 k are behind us... and we got some local press:
http://vf.is/Frettir/49061/default.aspx
http://mbl.is/frettir/innlent/2011/06/23/kafbatur_fra_islandi_til_kanari/
I have increased the number of yo’s to do to 7 (14 half yo’s).
also:
!put u_alt_min_depth 80
Auto-refreshing HYCOM forecast for Google Earth:
http://marine.rutgers.edu/~kerfoot/gearth/kmz/HYCOM/silboChallenger2011.kmz
Teledyne Webb Research, Rutgers University, PLOCAN, NOC partnership deployment.
Lithium batteries
Deployment notification:
Hello from Iceland!
Silbo has been deployed from the vessel Oddur V Gíslason (see attached) about 10 meters south of Grindavik Iceland in 130 meters of water. Deploying the glider was Chris DeCollibus from TWR assisted by Alvaro Lorenzo of Plocan and Arnar Steingrímsson of Teledyene Gavia.
Silbo is running the mission leif.mi. The first single dive will be to ~100 meters and then surface in the not to distant future, if all looks good with the data the next leg will be either 4 yo’s or 4.5 hrs, whichever comes first. I suggest we leave the buoyancy at the present +/- 250 until we get into the deeper water.
Tomorrow the plan is that Lauren will start to dial in the autoballast/speed control and when satisfied we will prune back the data in the sbd file. We might want to put the sensors pruned into and mbd to occasionally monitor them. The ebd is presently set to record CTD data every 16 seconds on downcast only.
Best of luck and thank you to all in advance for the work that will be put in!
Ben Allsup