Connection Event: Carrier Detect found. 9854 Iridium console active and ready... Vehicle Name: ru43 Curr Time: Sat Jun 14 02:59:47 2025 MT: 9854 DR Location: 3931.922 N -7313.218 E measured 745.303 secs ago GPS TooFar: 69696969.000 N 69696969.000 E measured 1e+308 secs ago GPS Invalid : 3931.061 N -7312.125 E measured 798.425 secs ago GPS Location: 3931.922 N -7313.218 E measured 748.015 secs ago sensor:c_wpt_lat(lat)=3934.1085 9790.28 secs ago sensor:c_wpt_lon(lon)=-7321.0128 9790.28 secs ago sensor:m_battery(volts)=15.9831527228067 668.411 secs ago sensor:m_coulomb_amphr(amp-hrs)=39.3138820000011 8.27 secs ago sensor:m_coulomb_amphr_total(amp-hrs)=39.513882000001 8.275 secs ago sensor:m_depth(m)=0.454905690283717 8.177 secs ago sensor:m_digifin_leakdetect_reading(nodim)=1023 0.048 secs ago sensor:m_gps_mag_var(rad)=0.226892802759263 748.061 secs ago sensor:m_iridium_attempt_num(nodim)=1 44.521 secs ago sensor:m_iridium_call_num(nodim)=1203 0.059 secs ago sensor:m_iridium_dialed_num(nodim)=1475 16.519 secs ago sensor:m_leakdetect_voltage(volts)=2.49065934065934 631.802 secs ago sensor:m_leakdetect_voltage_forward(volts)=2.49346764346764 631.767 secs ago sensor:m_leakdetect_voltage_science(volts)=2.49212454212454 631.732 secs ago sensor:m_tot_num_inflections(nodim)=30857 817.489 secs ago sensor:m_vacuum(inHg)=9.09322366300366 623.668 secs ago sensor:m_water_vx(m/s)=-0.046273435505276 765.399 secs ago sensor:m_water_vy(m/s)=0.024769982853674 765.402 secs ago sensor:u_max_altimeter(m)=200 1e+308 secs ago sensor:u_min_water_depth(m)=0 1e+308 secs ago sensor:u_use_current_correction(nodim)=1 1e+308 secs ago sensor:x_last_wpt_lat(lat)=3932.0118 1e+308 secs ago sensor:x_last_wpt_lon(lon)=-7304.8544 1e+308 secs ago ABORT HISTORY: total since reset: 1 ABORT HISTORY: last abort cause: MS_ABORT_OVERDEPTH ABORT HISTORY: last abort details: ABORT HISTORY: last abort time: 2025-06-05T16:04:07 ABORT HISTORY: last abort segment: ru43-2025-155-0-0 (0098.0000) ABORT HISTORY: last abort mission: od.mi 9854 No login script found for processing. 9930 66 SCI ERROR: science start logging failed GLD: ERROR resuming logging -------------------------------- Error from CmdDispatch():Error sending files 9930 ERROR behavior surface_3: S COMMAND FAILED: s -num=4 *.sbd *.tbd *.tcd *.scd *.vem *.azf *.asc *.obs *.mrd 10025 90 SCI:PROGLET house_elf begin() called 10025 SCI: house_elf: Version 1.2 10025 SCI:PROGLET ctd41cp begin() called 10025 SCI: ctd41cp: Version 0.2 10025 SCI: ctd41cp: Will be sending the following data to glider: 10025 SCI: sci_water_cond(s/m) 10025 SCI: sci_water_temp(degc) 10025 SCI: sci_water_pressure(bar) 10025 SCI: sci_ctd41cp_timestamp(timestamp) 10025 SCI:PROGLET flbbcd begin() called 10025 SCI: flbbcd: Version 0.0 10025 SCI: flbbcd: Will be sending following data to glider: 10025 SCI: sci_flbbcd_chlor_units(ug/l) 10025 SCI: sci_flbbcd_bb_units(nodim) 10025 SCI: sci_flbbcd_cdom_units(ppb) 10025 SCI: sci_flbbcd_chlor_sig(nodim) 10025 SCI: sci_flbbcd_bb_sig(nodim) 10025 SCI: sci_flbbcd_cdom_sig(nodim) 10025 SCI: sci_flbbcd_chlor_ref(nodim) 10025 SCI: sci_flbbcd_bb_ref(nodim) 10025 SCI: sci_flbbcd_cdom_ref(nodim) 10025 SCI: sci_flbbcd_therm(nodim) 10025 SCI: sci_flbbcd_timestamp(timestamp) 10025 SCI:Bit(0) raise count is now 0. 10025 SCI:Bit(0) raise count is now 0. 10025 SCI:PROGLET oxy4 begin() called 10025 SCI: oxy4: Version 0.0 10025 SCI: oxy4: Will be sending following data to glider: 10025 SCI: sci_oxy4_oxygen(um) 10025 SCI: sci_oxy4_saturation(%) 10025 SCI: sci_oxy4_temp(degc) 10025 SCI: sci_oxy4_calphase(deg) 10025 SCI: sci_oxy4_tcphase(deg) 10025 SCI: sci_oxy4_c1rph(deg) 10025 SCI: sci_oxy4_c2rph(deg) 10025 SCI: sci_oxy4_c1amp(mv) 10025 SCI: sci_oxy4_c2amp(mv) 10025 SCI: sci_oxy4_rawtemp(mv) 10025 SCI: sci_oxy4_timestamp(timestamp) 10025 SCI:Bit(2) raise count is now 0. 10025 SCI:Bit(2) raise count is now 0. 10025 SCI:PROGLET vr2c begin() called 10025 SCI:PROGLET dmon begin() called 10025 SCI: dmon: Version 0.0 10025 SCI: dmon: Will be sending following data to glider: 10025 SCI: sci_dmon_msg_byte_count(nodim) 10025 SCI:PROGLET house_elf start() called 10025 SCI: house_elf_run(): 0 error(s) in a row. (5 is fatal) 10025 SCI: house_elf_run(): 0 error(s) since house_elf_begin(). (50 is fatal) 10025 SCI:PROGLET vr2c start() called 10025 SCI: vr2c_run(): 0 error(s) in a row. (5 is fatal) 10025 SCI: vr2c_run(): 0 error(s) since vr2c_begin(). (50 is fatal) SCI ERROR: timed out waiting for science to stop logging 10051 95 ERROR behavior surface_3: Error from prepare_to_start_next_logging_segment() 10051 behavior surface_3: STATE Active -> ERROR 10051 ERROR behavior surface_3: Entered B_ERROR State ! 10051 ERROR behavior ?_-1: layered_control(): Behavior surface_3 entered B_ERROR state 10053 ERROR behavior ?_-1: abort_the_mission(0): (6)MS_ABORT_BEH_ERROR 10053 behavior ?_-1: abort_the_mission(): Changing U_CYCLE_TIME from 4.000000 to 15.000000 10053 save_and_change_sensors().... Changed u_depth_rate_filter_factor from 4 to -1 10053 Attempting to put everything back into service 10053 behavior ?_-1: Vehicle Name: ru43 10053 behavior ?_-1: abort_the_mission(): (6)MS_ABORT_BEH_ERROR 10053 behavior ?_-1: secs since abort started: 0 try num: 0 10053 behavior ?_-1: depths ini: 0 working: 102 at risk: 221 crush: 225 10053 behavior ?_-1: expected time/tries to surface: 306 20 10053 behavior ?_-1: max time/tries to go up: 300 20 10053 behavior ?_-1: too long: 0, not going up: 0, depth sensor busted:0 10053 behavior ?_-1: abort burn time/tries min: 600 40 10053 behavior ?_-1: abort burn time/tries max: 86400 5760 10053 behavior ?_-1: ABOVE WORKING DEPTH 10053 behavior ?_-1: drop_the_weight = 0 10053 Not recommended, but if in infinite loop, hit Control-C 10055 sensor: m_depth = 0.122047868124911 m 10055 96 Attempting to put only critical devices back into service 10055 behavior ?_-1: Vehicle Name: ru43 10055 behavior ?_-1: abort_the_mission(): (6)MS_ABORT_BEH_ERROR 10055 behavior ?_-1: secs since abort started: 2 try num: 1 10055 behavior ?_-1: depths ini: 0 working: 102 at risk: 221 crush: 225 10055 behavior ?_-1: expected time/tries to surface: 306 20 10055 behavior ?_-1: max time/tries to go up: 300 20 10055 behavior ?_-1: too long: 0, not going up: 0, depth sensor busted:0 10055 behavior ?_-1: abort burn time/tries min: 600 40 10055 behavior ?_-1: abort burn time/tries max: 86400 5760 10055 behavior ?_-1: ABOVE WORKING DEPTH 10055 behavior ?_-1: drop_the_weight = 0 10055 Not recommended, but if in infinite loop, hit Control-C 10057 sensor: m_depth = 0.321762561420195 m 10070 97 Attempting to put only critical devices back into service 10070 behavior ?_-1: Vehicle Name: ru43 10070 behavior ?_-1: abort_the_mission(): (6)MS_ABORT_BEH_ERROR 10070 behavior ?_-1: secs since abort started: 17 try num: 2 10070 behavior ?_-1: depths ini: 0 working: 102 at risk: 221 crush: 225 10070 behavior ?_-1: expected time/tries to surface: 306 20 10070 behavior ?_-1: max time/tries to go up: 300 20 10070 behavior ?_-1: too long: 0, not going up: 0, depth sensor busted:0 10070 behavior ?_-1: abort burn time/tries min: 600 40 10070 behavior ?_-1: abort burn time/tries max: 86400 5760 10070 ERROR behavior ?_-1: we_are_done(): At the surface, return (-2)MS_COMPLETED_ABNORMALLY 10070 behavior ?_-1: we_are_done(): Restoring U_CYCLE_TIME from 15.000000 to 4.000000 10070 restore_sensors().... Restored u_depth_rate_filter_factor from -1 to 4 10070 behavior ?_-1: ABOVE WORKING DEPTH 10070 behavior ?_-1: drop_the_weight = 0 10070 Not recommended, but if in infinite loop, hit Control-C 10071 behavior ?_-1: run_mission(): Mission completed: MS_COMPLETED_ABNORMALLY(-2) Vehicle Name: ru43 Mission Name: 100_n.mi Mission Number: ru43-2025-164-0-1 (0105.0001) post_mission_cleanup(): End of Mission timestamp: Sat Jun 14 03:03:27 2025 timestamp: Sat Jun 14 03:03:31 2025 Mission completed ABNORMALLY, ret = -3 Mission end: grun_mission() 100_n.mi ru43-2025-164-0-1 (0105.0001) SEQUENCE: 100_n.mi ru43-2025-164-0-1 (0105.0001) aborted on try 0 SEQUENCE: Forcing use of critical devices Returning to GliderDos to let iridium report in. Setting U_MAX_TIME_IN_GLIDERDOS(s) to 900 Command error: SEQUENCE: suspended GliderDos A 6 >why? ABORT HISTORY: total since reset: 2 ABORT HISTORY: last abort cause: MS_ABORT_BEH_ERROR ABORT HISTORY: last abort details: layered_control(): Behavior surface_3 entered B_ERROR state ABORT HISTORY: last abort time: 2025-06-14T03:03:04 ABORT HISTORY: last abort segment: ru43-2025-164-0-1 (0105.0001) ABORT HISTORY: last abort mission: 100_n.mi BOOT: Last reboot reason was REBOOT_POWER_DOWN - Power Down/Cold Boot Boot number : 233 CORE: Core dump present GliderDos A 6 > GliderDos A 6 >Put c_science_on 0 10197 28 sensor: c_science_on = 0 bool GliderDos A 6 >Put c_science_on 1 10214 32 sensor: c_science_on = 1 bool GliderDos A 6 >Glider-Science software version match: 10.080000 Science hardware version is 3.000000 10216 33 SCI:PROGLET house_elf begin() called 10216 SCI: house_elf: Version 1.2 10216 SCI:PROGLET ctd41cp begin() called 10216 SCI: ctd41cp: Version 0.2 10216 SCI: ctd41cp: Will be sending the following data to glider: 10216 SCI: sci_water_cond(s/m) 10216 SCI: sci_water_temp(degc) 10216 SCI: sci_water_pressure(bar) 10216 SCI: sci_ctd41cp_timestamp(timestamp) 10216 SCI:PROGLET flbbcd begin() called 10216 SCI: flbbcd: Version 0.0 10216 SCI: flbbcd: Will be sending following data to glider: 10216 SCI: sci_flbbcd_chlor_units(ug/l) 10216 SCI: sci_flbbcd_bb_units(nodim) 10216 SCI: sci_flbbcd_cdom_units(ppb) 10216 SCI: sci_flbbcd_chlor_sig(nodim) 10216 SCI: sci_flbbcd_bb_sig(nodim) 10216 SCI: sci_flbbcd_cdom_sig(nodim) 10216 SCI: sci_flbbcd_chlor_ref(nodim) 10216 SCI: sci_flbbcd_bb_ref(nodim) 10216 SCI: sci_flbbcd_cdom_ref(nodim) 10216 SCI: sci_flbbcd_therm(nodim) 10216 SCI: sci_flbbcd_timestamp(timestamp) 10216 SCI:Bit(0) raise count is now 0. 10216 SCI:Bit(0) raise count is now 0. 10216 SCI:PROGLET oxy4 begin() called 10216 SCI: oxy4: Version 0.0 10216 SCI: oxy4: Will be sending followi