Connection Event: Carrier Detect found.131383 Iridium console active and ready... Vehicle Name: ru38 Curr Time: Wed Jul 2 03:41:58 2025 MT: 131383 DR Location: 2638.480 N -8459.461 E measured 582.133 secs ago GPS TooFar: 69696969.000 N 69696969.000 E measured 1e+308 secs ago GPS Invalid : 2630.896 N -8456.779 E measured 629.092 secs ago GPS Location: 2638.480 N -8459.461 E measured 584.241 secs ago sensor:c_thruster_surface_depth(m)=0 450.439 secs ago sensor:c_wpt_lat(lat)=2708.87 450.61 secs ago sensor:c_wpt_lon(lon)=-8252.579 450.614 secs ago sensor:m_battery(volts)=14.5927831739961 3.7 secs ago sensor:m_coulomb_amphr(amp-hrs)=26.8499700000003 3.836 secs ago sensor:m_coulomb_amphr_total(amp-hrs)=436.140162999935 3.84 secs ago sensor:m_depth(m)=0 3.612 secs ago sensor:m_digifin_leakdetect_reading(nodim)=1022 0.05 secs ago sensor:m_gps_mag_var(rad)=0.059341194567807 584.291 secs ago sensor:m_iridium_attempt_num(nodim)=2 44.304 secs ago sensor:m_iridium_call_num(nodim)=1898 0.06 secs ago sensor:m_iridium_dialed_num(nodim)=2680 16.156 secs ago sensor:m_leakdetect_voltage(volts)=2.48675213675214 206.847 secs ago sensor:m_leakdetect_voltage_forward(volts)=2.5 206.811 secs ago sensor:m_leakdetect_voltage_science(volts)=2.5 206.775 secs ago sensor:m_tot_num_inflections(nodim)=5098 626.231 secs ago sensor:m_vacuum(inHg)=9.25050554334554 3.701 secs ago sensor:m_water_vel_dir(rad)=6.21157171517566 22533.3 secs ago sensor:m_water_vel_mag(m/s)=0.379849487791927 602.233 secs ago sensor:m_water_vx(m/s)=-0.12272780636575 602.237 secs ago sensor:m_water_vy(m/s)=0.35947672931699 602.241 secs ago sensor:u_alt_min_depth(m)=2 1e+308 secs ago sensor:u_use_current_correction(nodim)=0 22466.2 secs ago sensor:x_last_wpt_lat(lat)=2622.47 46701.8 secs ago sensor:x_last_wpt_lon(lon)=-8455.647 46701.8 secs ago ABORT HISTORY: total since reset: 1 ABORT HISTORY: last abort cause: MS_ABORT_NOINPUT ABORT HISTORY: last abort details: M_DEPTH not updating ABORT HISTORY: last abort time: 2025-07-02T03:39:57 ABORT HISTORY: last abort segment: ru38-2025-180-0-12 (0153.0012) ABORT HISTORY: last abort mission: 1k_n.mi GliderDos A 12 >131383 No login script found for processing. GliderDos A 12 > GliderDos A 12 >Report ++ m_depth GliderDos A 12 >131516 22 sensor: m_depth = 0.05 m 131520 23 sensor: m_depth = 0 m 131524 24 sensor: m_depth = 0 m 131528 25 sensor: m_depth = 1.30298925500209 m 131532 26 sensor: m_depth = 0 m 131536 27 sensor: m_depth = 0 m 131540 28 sensor: m_depth = 0 m 131544 29 sensor: m_depth = 0 m 131552 30 sensor: m_depth = 0 m 131556 31 sensor: m_depth = 0 m 131560 32 sensor: m_depth = 0 m not found>*.ma< [dockzr | dockszr] [?][-v N][-nosmartdir][-f rf | irid][-cd dir][-noremove] [-archive] [-d ] ... [[-d ... ] ... ] 131564 33 sensor: m_depth = 0 m Rep not found>*.dat< not found>*.ini< not found>*.cfg< [dockzr | dockszr] [?][-v N][-nosmartdir][-f rf | irid][-cd dir][-noremove] [-archive] [-d ] ... [[-d ... ] ... ]