Connection Event: Carrier Detect found.349.71 Iridium console active and ready... Vehicle Name: ru32 Curr Time: Thu Jul 31 13:27:54 2025 MT: 349 DR Location: 3902.880 N -7421.011 E measured 1e+308 secs ago GPS TooFar: 69696969.000 N 69696969.000 E measured 1e+308 secs ago GPS Invalid : 3902.623 N -7419.337 E measured 1e+308 secs ago GPS Location: 3902.880 N -7421.008 E measured 1e+308 secs ago sensor:c_wpt_lat(lat)=3903.216 1e+308 secs ago sensor:c_wpt_lon(lon)=-7436.7607 1e+308 secs ago sensor:m_battery(volts)=14.6449481515075 4.282 secs ago sensor:m_coulomb_amphr(amp-hrs)=101.446937561035 4.478 secs ago sensor:m_coulomb_amphr_total(amp-hrs)=101.699062561188 4.496 secs ago sensor:m_depth(m)=1.75473779203822 4.364 secs ago sensor:m_digifin_leakdetect_reading(nodim)=1022 0.596 secs ago sensor:m_gps_mag_var(rad)=0.216420827247297 1e+308 secs ago sensor:m_iridium_attempt_num(nodim)=1 41.481 secs ago sensor:m_iridium_call_num(nodim)=6333 0.686 secs ago sensor:m_iridium_dialed_num(nodim)=8713 17.056 secs ago sensor:m_leakdetect_voltage(volts)=2.48577533577534 4.44 secs ago sensor:m_leakdetect_voltage_forward(volts)=2.49136141636142 4.463 secs ago sensor:m_leakdetect_voltage_science(volts)=-1 4.501 secs ago sensor:m_tot_num_inflections(nodim)=119984 1e+308 secs ago sensor:m_vacuum(inHg)=8.09566895604396 4.892 secs ago sensor:m_water_vx(m/s)=-0.0138806354000167 1e+308 secs ago sensor:m_water_vy(m/s)=0.00224932071334615 1e+308 secs ago sensor:u_max_altimeter(m)=8 1e+308 secs ago sensor:u_min_water_depth(m)=0 1e+308 secs ago sensor:u_use_current_correction(nodim)=1 1e+308 secs ago sensor:x_last_wpt_lat(lat)=3902.9223 1e+308 secs ago sensor:x_last_wpt_lon(lon)=-7419.0801 1e+308 secs ago ABORT HISTORY: total since reset: 5 ABORT HISTORY: last abort cause: MS_ABORT_BEH_ERROR ABORT HISTORY: last abort details: layered_control(): Behavior yo_6 entered B_ERROR state pitch_motor not InService ABORT HISTORY: last abort time: 2025-07-31T13:22:50 ABORT HISTORY: last abort segment: ru32-2025-211-1-0 (0254.0000) ABORT HISTORY: last abort mission: 100_NOBAT.MI 351.16 No login script found for processing. 351.19 DRIVER_ODDITY:iridium:1516:xxx_ctrl() ran too long get m_battpos = 0.586188 in GliderDos A 6 >get c_battpos = 0.850000 in GliderDos A 6 >put c_battpos 0.5 397.42 77 sensor: c_battpos = 0.5 in GliderDos A 6 >report ++ m_battpos GliderDos A 6 >407.22 80 sensor: m_battpos = 0.586188034188034 in 411.25 81 sensor: m_battpos = 0.586188034188034 in 415.34 82 sensor: m_battpos = 0.584824175824176 in 419.42 83 sensor: m_battpos = 0.586188034188034 in 423.50 84 sensor: m_battpos = 0.586188034188034 in 427.58 85 sensor: m_battpos = 0.586188034188034 in put c_battpos 0.7 434.50 sensor: c_battpos = 0.7 in GliderDos A 6 >435.46 88 sensor: m_battpos = 0.586188034188034 in 439.50 89 sensor: m_battpos = 0.586188034188034 in 443.59 90 sensor: m_battpos = 0.586188034188034 in 447.61 91 sensor: m_battpos = 0.584824175824176 in 451.69 92 sensor: m_battpos = 0.586188034188034 in 455.76 93 sensor: m_battpos = 0.586188034188034 in whack Bad command or file name GliderDos A 6 >458.84 94 sensor: m_battpos = 0.586188034188034 in 462.86 95 sensor: m_battpos = 0.586188034188034 in 466.94 96 sensor: m_battpos = 0.586188034188034 in 474.65 97 sensor: m_battpos = 0.586188034188034 in 478.68 98 sensor: m_battpos = 0.586188034188034 in 482.77 99 sensor: m_battpos = 0.586188034188034 in 486.85 0 sensor: m_battpos = 0.586188034188034 in report clearall GliderDos A 6 >put u_max_time_in_gliderdos 3600 528.64 9 sensor: u_max_time_in_gliderdos = 3600 sec GliderDos A 6 > Vehicle Name: ru32 528.69 NOTE:GPS fix is getting stale: NEVER HAD A FIX GliderDos A 6 >callback 3 I am going to hangup the Iridium! I will call you back in 3 minutes at the primary number ( 88160000592 ) GliderDos A 6 >539.26 12 disabling Iri