Connection Event: Carrier Detect found.1196347    Iridium console active and ready...
Vehicle Name: ru29
Curr Time: Fri Oct 10 00:20:38 2025 MT: 1196345
DR  Location:  1303.816 N -5955.598 E measured      41.39 secs ago
GPS TooFar:   69696969.000 N 69696969.000 E measured     1e+308 secs ago
GPS Invalid :  1303.453 N -5954.815 E measured    104.328 secs ago
GPS Location:  1303.816 N -5955.598 E measured     43.806
not found>*.ma<
[dockzr | dockszr] [?][-v N][-nosmartdir][-f rf | irid][-cd dir][-noremove] [-archive]
  [-d ]   ... 
  [[-d    ... ] ... ]
 secs ago
   sensor:c_thruster_surface_depth(m)=0           19665.8 secs ago
   sensor:c_wpt_lat(lat)=1303.665                  68.718 secs ago
   sensor:c_wpt_lon(lon)=-5954.158                 68.785 secs ago
   sensor:m_battery(volts)=14.7037048304446        48.208 secs ago
   sensor:m_coulomb_amphr(amp-hrs)=432.171630859375      5.312 secs ago
   sensor:m_coulomb_amphr_total(amp-hrs)=435.674754859451      5.333 secs ago
   sensor:m_depth(m)=0.0996019872967208             5.278 secs ago
   sensor:m_digifin_leakdetect_reading(nodim)=1022      0.688 secs ago
   sensor:m_gps_mag_var(rad)=0.267035375555132     44.367 secs ago
   sensor:m_iridium_attempt_num(nodim)=1           38.987 secs ago
   sensor:m_iridium_call_num(nodim)=8837            0.753 secs ago
   sensor:m_iridium_dialed_num(nodim)=14728        10.583 secs ago
   sensor:m_leakdetect_voltage(volts)=2.47786935286935     29.092 secs ago
   sensor:m_leakdetect_voltage_forward(volts)=2.48565323565324     29.118 secs ago
   sensor:m_leakdetect_voltage_science(volts)=-1      5.785 secs ago
   sensor:m_tot_num_inflections(nodim)=37229      113.163 secs ago
   sens
not found>*.dat<
not found>*.ini<
not found>*.cfg<
not found>*.0<
not found>*.1<
[dockzr | dockszr] [?][-v N][-nosmartdir][-f rf | irid][-cd dir][-noremove] [-archive]
  [-d ]   ... 
  [[-d    ... ] ... ]
or:m_vacuum(inHg)=8.39392237484737          58.727 secs ago
   sensor:m_water_vx(m/s)=-0.110593808626611       71.998 secs ago
   sensor:m_water_vy(m/s)=0.0226955476148539        72.04 secs ago
   sensor:m_why_started(enum)=64                   1e+308 secs ago
   sensor:u_alt_min_depth(m)=500                   1e+308 secs ago
   sensor:u_min_water_depth(m)=0                   1e+308 secs ago
   sensor:u_use_current_correction(nodim)=1        1e+308 secs ago
   sensor:x_last_wpt_lat(lat)=1303.665             70.213 secs ago
   sensor:x_last_wpt_lon(lon)=-5955.806             70.27 secs ago
ABORT HISTORY: total since reset: 4
ABORT HISTORY: last abort cause: MS_ABORT_BEH_ERROR
ABORT HISTORY: last abort details: layered_control(): Behavior surface_2 entered B_ERROR state 
ABORT HISTORY: last abort time: 2025-09-26T03:56:31
ABORT HISTORY: last abort segment: ru29-2025-250-0-283 (0749.0283)
ABORT HISTORY: last abort mission: 1K_N.MI
1196348    No login script found for processing.
1196348    DRIVER_ODDITY:iridium:1785:xxx_ctrl() ran too long
Glider ru29 at surface.
Because:nothing commanded [behavior surface_2 start_when = 1.0]
MissionName:1K_N.MI MissionNum:ru29-2025-268-0-180 (0750.0180)
Vehicle Name: ru29
Curr Time: Fri Oct 10 00:21:17 2025 MT: 1196385
DR  Location:  1303.816 N -5955.598 E measured     80.595 secs ago
GPS TooFar:   69696969.000 N 69696969.000 E measured     1e+308 secs ago
GPS Invalid :  1303.453 N -5954.815 E measured    143.533 secs ago
GPS Location:  1303.816 N -5955.598 E measured      83.01 secs ago
   sensor:c_thruster_surface_depth(m)=0             19705 secs ago
   sensor:c_wpt_lat(lat)=1303.665                 107.875 secs ago
   sensor:c_wpt_lon(lon)=-5954.158                107.916 secs ago
   sensor:m_battery(volts)=14.6821216489874        24.408 secs ago
   sensor:m_coulomb_amphr(amp-hrs)=432.176361083984      4.502 secs ago
   sensor:m_coulomb_amphr_total(amp-hrs)=435.679485084061      4.516 secs ago
   sensor:m_depth(m)=0.376274174232259              4.441 secs ago
   sensor:m_digifin_leakdetect_reading(nodim)=1022      9.317 secs ago
   sensor:m_gps_mag_var(rad)=0.267035375555132     83.437 secs ago
   sensor:m_iridium_attempt_num(nodim)=1           78.041 secs ago
   sensor:m_iridium_call_num(nodim)=8837           39.788 secs ago
   sensor:m_iridium_dialed_num(nodim)=14728        49.608 secs ago
   sensor:m_leakdetect_voltage(volts)=2.4778083028083      4.612 secs ago
   sensor:m_leakdetect_voltage_forward(volts)=2.48553113553114      4.628 secs ago
   sensor:m_leakdetect_voltage_science(volts)=-1      4.659 secs ago
   sensor:m_tot_num_inflections(nodim)=37229      152.156 secs ago
   sensor:m_vacuum(inHg)=8.84441202686202          34.536 secs ago
   sensor:m_water_vx(m/s)=-0.110593808626611      110.965 secs ago
   sensor:m_water_vy(m/s)=0.0226955476148539      110.997 secs ago
   sensor:m_why_started(enum)=64                   1e+308 secs ago
   sensor:u_alt_min_depth(m)=500                   1e+308 secs ago
   sensor:u_min_water_depth(m)=0                   1e+308 secs ago
   sensor:u_use_current_correction(nodim)=1        1e+308 secs ago
   sensor:x_last_wpt_lat(lat)=1303.665            109.038 secs ago
   sensor:x_last_wpt_lon(lon)=-5955.806           109.075 secs ago
devices:(t/m/s) errs:   1/   0/   0 warn:  40/   2/   0 odd:3614/ 460/   6
ABORT HISTORY: total since reset: 4
ABORT HISTORY: last abort cause: MS_ABORT_BEH_ERROR
ABORT HISTORY: last abort details: layered_control(): Behavior surface_2 entered B_ERROR state 
ABORT HISTORY: last abort time: 2025-09-26T03:56:31
ABORT HISTORY: last abort segment: ru29-2025-250-0-283 (0749.0283)
ABORT HISTORY: last abort mission: 1K_N.MI
   Hit Control-R to RESUME the mission, i.e. dive!
   Hit Control-C to END    the mission, i.e. GliderDos
   Hit Control-E to extend surface time by 5 minutes.
   Hit Control-W to get device warning reports.
   Hit Control-F to re-read yo, goto_l, surface, sample, drift_ mafiles.
   Hit H  <0:1> to Hangup and call back in  minutes at 0-primary 1-alternate number.
   Hit S [-f={rf}|{irid] [-num=] [-t=] [filespec ...] to send log files
   Hit !   to execute 
   Hit Control-T to consci to science computer when comms ready:
                                               ... communications ready for consci.
Water Velocity Calculations waiting for final gps fix(ideally -71 secs)
Waypoint: (1303.6650,-5954.1580) Range: 2626m, Bearing: 112deg, Age: 0:1h:m
Time until diving is: 210 secs
s -num=2 *.sbd *.tbd *.tcd *.scd
--------------------------------
1196409 48 07500180.mlg LOG FILE CLOSED
SCIENCE DATA LOGGING: science IS running
CONSCI REQUESTED (using IRIDIUM as console)
ASKING SCIENCE COMPUTER TO SWITCH TO COMMAND MODE via IRIDIUM
SWITCHING TO SCIENCE COMMAND MODE over IRIDIUM
Normal operation resumes when:
    SciDos> QUIT              -or-
    Lose CD (unplug freewave/hangup iridium) -or-
    run longer than U_SCI_CMD_MAX_CONSCI_TIME(28800)s
1196418 51 Neutering the Freewave Console
SCI: Implicitly limiting total transfer to 28800 secs, representing 2880 KB total size
SCI: Enumerating and selecting files
SCI: About to send 2 files
Prechecking is not necessary for this invocation
START
**B00000000000000
Starting zModem transfer of 07500180.tbd to/from ru29 size is 13845