Connection Event: Carrier Detect found. 55704 Iridium console active and ready... Vehicle Name: REDWING Curr Time: Wed Dec 17 16:46:41 2025 MT: 55704 DR Location: 3918.119 N -4553.779 E measured 620.445 secs ago GPS TooFar: 69696969.000 N 69696969.000 E measured 1e+308 secs ago GPS Invalid : 3907.911 N -4602.889 E measured 717.613 secs ago GPS Location: 3918.119 N -4553.779 E measured 621.826 secs ago sensor:c_autoballast_state(enum)=2 1028.5 secs ago sensor:c_climb_bpump(X)=675 1021.43 secs ago sensor:c_dive_bpump(X)=-525 1021.43 secs ago sensor:c_iridium_current_num(enum)=0 24283.1 secs ago sensor:c_wpt_lat(lat)=3900 55663.3 secs ago sensor:c_wpt_lon(lon)=-4200 55663.4 secs ago sensor:m_avg_climb_rate(m/s)=-0.222175149425918 813.548 secs ago sensor:m_avg_dive_rate(m/s)=0.271512060246676 4603.15 secs ago sensor:m_battery(volts)=30.4318894920233 0.341 secs ago sensor:m_battery_amp_hours_remaining(amp-hrs)=568.58984375 0.345 secs ago sensor:m_cycle_overruns(int)=3834 84.826 secs ago sensor:m_digifin_leakdetect_reading(nodim)=952 1.453 secs ago sensor:m_dist_to_wpt(m)=338237.308380831 620.51 secs ago sensor:m_gps_dist_segment(km)=23.0253874641384 685.551 secs ago sensor:m_inflection_depth(m)=911.516346577341 4494.91 secs ago sensor:m_iridium_attempt_num(nodim)=1 56.085 secs ago sensor:m_iridium_signal_strength(nodim)=4 16.082 secs ago sensor:m_leakdetect_voltage(volts)=2.48690476190476 11.904 secs ago sensor:m_leakdetect_voltage_forward(volts)=2.48946886446886 11.868 secs ago sensor:m_leakdetect_voltage_science(volts)=2.49246031746032 11.833 secs ago sensor:m_leakdetect_voltage_stack_on(volts)=2.48775946275946 11.797 secs ago sensor:m_lithium_battery_relative_charge(%)=62.9166666666667 0.393 secs ago sensor:m_sci_cycle_overruns(int)=0 1e+308 secs ago sensor:m_system_errors(int)=0 0.16 secs ago sensor:m_tot_num_inflections(nodim)=6439 809.619 secs ago sensor:m_vacuum(inHg)=7.93335282051282 16.017 secs ago sensor:m_water_vx(m/s)=0.380096259536626 685.603 secs ago sensor:m_water_vy(m/s)=0.525654630845568 685.605 secs ago sensor:u_alt_min_depth(m)=1200 1e+308 secs ago sensor:u_low_power_cycle_time(sec)=30 1e+308 secs ago sensor:u_use_current_correction(nodim)=2 1e+308 secs ago sensor:x_last_wpt_lat(lat)=3947.154 1e+308 secs ago sensor:x_last_wpt_lon(lon)=-7026.586 1e+308 secs ago sensor:x_surface_active(nodim)=4 1028.63 secs ago ABORT HISTORY: total since reset: 15 ABORT HISTORY: last abort cause: MS_ABORT_DEVICE_ERROR ABORT HISTORY: last abort details: The thruster device driver returned an error. ABORT HISTORY: last abort time: 2025-12-17T01:06:57 ABORT HISTORY: last abort segment: REDWING-2025-347-0-18 (0137.0018) ABORT HISTORY: last abort mission: redwing.mi 55704 No login script found for processing. GliderMIS 534> > 55708 68 sensor: c_thruster_on = 0 % 55712 69 sensor: c_thruster_on = 0 % 55712 DRIVER_ODDITY:digifin:8:FIN_POS_INCORRECT 55716 70 sensor: c_thruster_on = 0 % 55720 71 sensor: c_thruster_on = 0 % ^EExtending surface time by 5 minutes 55724 72 sensor: c_thruster_on = 0 % I heard a character ('CR'), but not the right one Drained the following 4 pending chars from input buffer: 05 0d 05 0d ^E CR ^E CR .... 55728 73 sensor: c_thruster_on = 0 % 55736 74 sensor: c_thruster_on = 0 % GliderMIS 802> > 55740 75 sensor: c_thruster_on = 0 % 55744 76 sensor: c_thruster_on = 0 % 55748 77 sensor: c_thruster_on = 0 % 55752 78 sensor: c_thruster_on = 0 % 55753 DRIVER_ODDITY:digifin:8:FIN_POS_INCORRECT !use - thruster (null) -------------------------------- thruster:ok -------------------------------- 55758 79 behavior surface_4: ! succeeded:use - thruster 55758 behavior surface_4: SUBSTATE 7 ->7 : After ! command, waiting for control-C to exit/resume 55758 sensor: c_thruster_on = 0 % 55760 80 sensor: c_thruster_on = 0 % 55764 81 sensor: c_thruster_on = 0 % 55768 82 sensor: c_thruster_on = 0 % !use (null) -------------------------------- name in ALLCAPS means CRITICAL device (* => SUPERCRITICAL) [I Installed] [- Not_Installed] [u In_use] [- Not_In_use] [X Out_of_Service] name limits stats (#total/#mission/#segment) os w/s w/m os errors warnings oddities 0 simdrvr - 1 test_driver - 2 ARGOS* I u -1 20 5 0 3 WATCHDOG I u -1 -1 -1 0 4 DEADMAN I u -1 20 5 0 5 CONSOLE* I u -1 20 5 0 6 attitude_rev I u 3 20 5 0 7 ocean_pressure I u 3 20 5 0 8 vacuum I u 3 20 5 0 9 bms I u 3 20 5 0 [ 0 0 0] [ 0 0 0] [ 330 0 0] 10 HOTEL I u 3 20 5 0 11 air_pump I u 3 20 5 0 12 pitch_motor I u 3 20 5 0 [ 0 0 0] [ 7 0 0] [1965 0 0] 13 science_super I u 3 20 5 0 [ 0 0 0] [ 1 0 0] [ 197 0 0] 14 digifin I u 3 20 5 0 [ 0 0 0] [ 0 0 0] [5344 5 5] 15 GPS I u -1 20 5 0 [ 0 0 0] [ 14 0 0] [ 0 0 0] 16 GPS_SAASM - 17 altimeter I u 3 20 5 0 18 altimeter_232 - 19 IRIDIUM* I u -1 20 5 0 [ 0 0 0] [ 0 0 0] [ 706 0 0] 20 leakdetect I u 3 20 5 0 21 recovery - 22 veh_temp I u 3 20 5 0 23 HD_PUMP I u 3 20 5 0 [ 0 0 0] [ 0 0 0] [ 33 0 0] 24 thruster I - 3 20 5 2 [ 2 0 0] [ 15 3 3] [ 0 0 0] devices:(t/m/s) errs: 2/ 0/ 0 warn: 37/ 3/ 3 odd:8575/ 5/ 5 -------------------------------- 55774 83 behavior surface_4: ! succeeded:use 55774 behavior surface_4: SUBSTATE 7 ->7 : After ! command, waiting for control-C to exit/resume 55774 sensor: c_thruster_on = 0 % 55776 84 sensor: c_thruster_on = 0 % 55780 85 sensor: c_thruster_on = 0 % 55784 86 sensor: c_thruster_on = 0 % 55788 87 sensor: c_thruster_on = 0 % 55792 88 sensor: c_thruster_on = 0 % !put c_thruster_on 0 (null) -------------------------------- 55800 89 sensor: c_thruster_on = 0 % -------------------------------- 55800 behavior surface_4: ! succeeded:put c_thruster_on 0 55800 behavior surface_4: SUBSTATE 7 ->7 : After ! command, waiting for control-C to exit/resume 55800 sensor: c_thruster_on = 0 % 55800 90 sensor: c_thruster_on = 0 % 55804 91 sensor: c_thruster_on = 0 % 55805 DRIVER_ODDITY:digifin:8:FIN_POS_INCORRECT 55808 92 sensor: c_thruster_on = 0 % !report list (null) -------------------------------- ++ c_thruster_on = 0.000000 % ++ m_gps_ignored_lat = 3918.085700 lat ++ m_gps_ignored_lon = -4553.792200 lon ++ m_gps_invalid_lat = 3907.911400 lat ++ m_gps_invalid_lon = -4602.888700 lon ++ m_gps_lat = 3918.119000 lat ++ m_gps_lon = -4553.778600 lon ++ m_gps_status = 0.000000 enum ++ m_thruster1_current = 0.000000 amp ++ m_thruster2_current = 0.000000 amp -------------------------------- 55812 93 behavior surface_4: ! succeeded:report list 55812 behavior surface_4: SUBSTATE 7 ->7 : After ! command, waiting for control-C to exit/resume 55813 sensor: c_thruster_on = 0 % 55816 94 sensor: c_thruster_on = 0 % 55820 95 sensor: c_thruster_on = 0 % 55821 DRIVER_ODDITY:digifin:8:FIN_POS_INCORRECT !report clearall (null) -------------------------------- -------------------------------- 55828 96 behavior surface_4: ! succeeded:report clearall 55828 behavior surface_4: SUBSTATE 7 ->7 : After ! command, waiting for control-C to exit/resume 55844 0 DRIVER_ODDITY:digifin:8:FIN_POS_INCORRECT u I heard a character ('u'), but not the right one Drained the following 7 pending chars from input buffer: 73 65 20 61 6c 6c 0d s e SP a l l CR se all. GliderMIS 867> > 55860 4 DRIVER_ODDITY:digifin:8:FIN_POS_INCORRECT 55872 7 DRIVER_ODDITY:digifin:8:FIN_POS_INCORRECT ^C 55876 8 behavior surface_4: User Hit a Control-C, terminating the mission 55876 behavior surface_4: STATE Active -> Mission Complete 55876 behavior ?_-1: layered_control(): Mission completed normally 55876 behavior ?_-1: run_mission(): Mission completed: MS_COMPLETED_NORMALLY(-1) Vehicle Name: REDWING Mission Name: redwing.mi Mission Number: REDWING-2025-350-0-2 (0138.0002) post_mission_cleanup(): End of Mission timestamp: Wed Dec 17 16:49:39 2025 55883 01380002.mlg LOG FILE CLOSED timestamp: Wed Dec 17 16:49:43 2025 Mission completed normally Mission end: grun_mission() redwing.mi REDWING-2025-350-0-2 (0138.0002) SEQUENCE: redwing.mi REDWING-2025-350-0-2 (0138.0002) completed normally SEQUENCE: AAH redwing.mi mission finished normally AAH: M_RETRY_ABORT_COUNTER=2 AAH: resetting due to normal completion. Returning to GliderDos to let iridium report in. Setting U_MAX_TIME_IN_GLIDERDOS(s) to 900 GliderDos N -1 >^@^C GliderDos N -1 >use name in ALLCAPS means CRITICAL device (* => SUPERCRITICAL) [I Installed] [- Not_Installed] [u In_use] [- Not_In_use] [X Out_of_Service] name limits stats (#total/#mission/#segment) os w/s w/m os errors warnings oddities 0 simdrvr - 1 test_driver - 2 ARGOS* I u -1 20 5 0 3 WATCHDOG I u -1 -1 -1 0 4 DEADMAN I u -1 20 5 0 5 CONSOLE* I u -1 20 5 0 6 attitude_rev I u 3 20 5 0 7 ocean_pressure I u 3 20 5 0 8 vacuum I u 3 20 5 0 9 bms I u 3 20 5 0 [ 0 0 0] [ 0 0 0] [ 330 0 0] 10 HOTEL I u 3 20 5 0 11 air_pump I u 3 20 5 0 12 pitch_motor I u 3 20 5 0 [ 0 0 0] [ 7 0 0] [1965 0 0] 13 science_super I u 3 20 5 0 [ 0 0 0] [ 1 0 0] [ 197 0 0] 14 digifin I u 3 20 5 0 [ 0 0 0] [ 0 0 0] [5349 10 10] 15 GPS I u -1 20 5 0 [ 0 0 0] [ 14 0 0] [ 0 0 0] 16 GPS_SAASM - 17 altimeter I u 3 20 5 0 18 altimeter_232 - 19 IRIDIUM* I u -1 20 5 0 [ 0 0 0] [ 0 0 0] [ 706 0 0] 20 leakdetect I u 3 20 5 0 21 recovery - 22 veh_temp I u 3 20 5 0 23 HD_PUMP I u 3 20 5 0 [ 0 0 0] [ 0 0 0] [ 33 0 0] 24 thruster I - 3 20 5 2 [ 2 0 0] [ 15 3 3] [ 0 0 0] devices:(t/m/s) errs: 2/ 0/ 0 warn: 37/ 3/ 3 odd:8580/ 10/ 10 GliderDos N -1 >use all ok Exiting all devices ... 55919 18 disabling Iridium console...