Connection Event: Carrier Detect found.2154526 Iridium console active and ready...
Vehicle Name: REDWING
Curr Time: Fri Nov 28 19:24:10 2025 MT: 2154527
DR Location: 3900.471 N -5444.281 E measured 69.1 secs ago
GPS TooFar: 69696969.000 N 69696969.000 E measured 1e+308 secs ago
GPS Invalid : 3900.730 N -5449.336 E measured 160.626 secs ago
GPS Location: 3900.471 N -5444.281 E measured 70.353 secs ago
sensor:c_autoballast_state(enum)=2 601.717 secs ago
sensor:c_climb_bpump(X)=675 595.139 secs ago
sensor:c_dive_bpump(X)=-525 595.142 secs ago
sensor:c_iridium_current_num(enum)=0 38282 secs ago
sensor:c_wpt_lat(lat)=3800 669236 secs ago
sensor:c_wpt_lon(lon)=-5000 669236 secs ago
sensor:m_avg_climb_rate(m/s)=-0.13986257004625 233.248 secs ago
sensor:m_avg_dive_rate(m/s)=0.144050314924387 5647.1 secs ago
sensor:m_battery(volts)=30.8139210405274 1.214 secs ago
sensor:m_battery_amp_hours_remaining(amp-hrs)=642.3984375 1.218 secs ago
sensor:m_cycle_overruns(int)=3393 595.168 secs ago
sensor:m_digifin_leakdetect_reading(nodim)=951 1.125 secs ago
sensor:m_dist_to_wpt(m)=447927.85589852 69.164 secs ago
sensor:m_gps_dist_segment(km)=7.74168143690314 133.185 secs ago
sensor:m_inflection_depth(m)=906.893730823535 5490.23 secs ago
sensor:m_iridium_attempt_num(nodim)=2 36.081 secs ago
sensor:m_iridium_signal_strength(nodim)=4 24.084 secs ago
sensor:m_leakdetect_voltage(volts)=2.48696581196581 47.851 secs ago
sensor:m_leakdetect_voltage_forward(volts)=2.48928571428571 47.815 secs ago
sensor:m_leakdetect_voltage_science(volts)=2.49270451770452 47.78 secs ago
sensor:m_leakdetect_voltage_stack_on(volts)=2.48769841269841 47.744 secs ago
sensor:m_lithium_battery_relative_charge(%)=71.1666666666667 1.266 secs ago
sensor:m_sci_cycle_overruns(int)=0 1e+308 secs ago
sensor:m_system_errors(int)=0 0.16 secs ago
sensor:m_tot_num_inflections(nodim)=6127 229.318 secs ago
sensor:m_vacuum(inHg)=7.71799560439561 52.937 secs ago
sensor:m_water_vx(m/s)=-0.105550807871658 133.236 secs ago
sensor:m_water_vy(m/s)=0.090284665571175 133.24 secs ago
sensor:u_alt_min_depth(m)=1200 1e+308 secs ago
sensor:u_low_power_cycle_time(sec)=30 1e+308 secs ago
sensor:u_use_current_correction(nodim)=0 1.97377e+06 secs ago
sensor:x_last_wpt_lat(lat)=3947.154 1e+308 secs ago
sensor:x_last_wpt_lon(lon)=-7026.586 1e+308 secs ago
sensor:x_surface_active(nodim)=4 601.84 secs ago
ABORT HISTORY: total since reset: 13
ABORT HISTORY: last abort cause: MS_ABORT_BEH_ERROR
ABORT HISTORY: last abort details: layered_control(): Behavior surface_4 entered B_ERROR state
ABORT HISTORY: last abort time: 2025-11-03T20:41:35
ABORT HISTORY: last abort segment: REDWING-2025-306-2-0 (0135.0000)
ABORT HISTORY: last abort mission: redwing.mi
2154527 No login script found for processing.
2154542 87 DRIVER_ODDITY:digifin:8:FIN_POS_INCORRECT
GliderMIS 501>
!where
(null)
--------------------------------
Vehicle Name: REDWING
Curr Time: Fri Nov 28 19:24:39 2025 MT: 2154555
DR Location: 3900.471 N -5444.281 E measured 98.285 secs ago
GPS TooFar: 69696969.000 N 69696969.000 E measured 1e+308 secs ago
GPS Invalid : 3900.730 N -5449.336 E measured 189.812 secs ago
GPS Location: 3900.471 N -5444.281 E measured 99.539 secs ago
sensor:c_autoballast_state(enum)=2 630.902 secs ago
sensor:c_climb_bpump(X)=675 624.324 secs ago
sensor:c_dive_bpump(X)=-525 624.328 secs ago
sensor:c_iridium_current_num(enum)=0 382849 secs ago
sensor:c_wpt_lat(lat)=3800 669265 secs ago
sensor:c_wpt_lon(lon)=-5000 669265 secs ago
sensor:m_avg_climb_rate(m/s)=-0.13986257004625 262.433 secs ago
sensor:m_avg_dive_rate(m/s)=0.144050314924387 5676.28 secs ago
sensor:m_battery(volts)=30.8339707264524 0.899 secs ago
sensor:m_battery_amp_hours_remaining(amp-hrs)=642.3984375 0.903 secs ago
sensor:m_cycle_overruns(int)=3393 624.353 secs ago
sensor:m_digifin_leakdetect_reading(nodim)=951 0.811 secs ago
sensor:m_dist_to_wpt(m)=447927.85589852 98.349 secs ago
sensor:m_gps_dist_segment(km)=7.74168143690314 162.37 secs ago
sensor:m_inflection_depth(m)=906.893730823535 5519.41 secs ago
sensor:m_iridium_attempt_num(nodim)=0 0.08 secs ago
sensor:m_iridium_signal_strength(nodim)=4 53.268 secs ago
sensor:m_leakdetect_voltage(volts)=2.48678266178266 13.078 secs ago
sensor:m_leakdetect_voltage_forward(volts)=2.48956043956044 13.042 secs ago
sensor:m_leakdetect_voltage_science(volts)=2.49276556776557 13.007 secs ago
sensor:m_leakdetect_voltage_stack_on(volts)=2.48769841269841 12.971 secs ago
sensor:m_lithium_battery_relative_charge(%)=71.1666666666667 0.951 secs ago
sensor:m_sci_cycle_overruns(int)=0 1e+308 secs ago
sensor:m_system_errors(int)=0 5.345 secs ago
sensor:m_tot_num_inflections(nodim)=6127 258.502 secs ago
sensor:m_vacuum(inHg)=7.71799560439561 82.122 secs ago
sensor:m_water_vx(m/s)=-0.105550807871658 162.42 secs ago
sensor:m_water_vy(m/s)=0.090284665571175 162.424 secs ago
sensor:u_alt_min_depth(m)=1200 1e+308 secs ago
sensor:u_low_power_cycle_time(sec)=30 1e+308 secs ago
sensor:u_use_current_correction(nodim)=0 1.9738e+06 secs ago
sensor:x_last_wpt_lat(lat)=3947.154 1e+308 secs ago
sensor:x_last_wpt_lon(lon)=-7026.586 1e+308 secs ago
sensor:x_surface_active(nodim)=4 631.024 secs ago
--------------------------------
2154556 90 behavior surface_4: ! succeeded:where
2154556 behavior surface_4: SUBSTATE 7 ->7 : After ! command, waiting for control-C to exit/resume
2154582 96 DRIVER_ODDITY:digifin:8:FIN_POS_INCORRECT
GliderMIS 568>
not found>*<
[dockzr | dockszr] [?][-v N][-nosmartdir][-f rf | irid][-cd dir][-noremove] [-archive]
[-d ] ...
[[-d ... ] ... ]
GliderMIS 536>
not found>*<
[dockzr | dockszr] [?][-v N][-nosmartdir][-f rf | irid][-cd dir][-noremove] [-archive]
[-d ] ...
[[-d ... ] ... ]
2154630 8 DRIVER_ODDITY:digifin:8:FIN_POS_INCORRECT
GliderMIS 504>
s *.sbd *.tbd
(null)
--------------------------------
2154656 14 01360209.mlg LOG FILE CLOSED
2154660 15 GLD: Enumerating and selecting files
About to send 2 files
Prechecking is not necessary for this invocation
selected IRIDIUM
2154661 save_and_change_sensors()....
Changed u_use_ctd_depth_for_flying from 0 to 0
2154661 save_and_change_sensors()....
Changed c_science_printout from 0 to 0
Waiting for motors idle
START
**B00000000000000
Starting zModem transfer of 01360209.sbd to/from redwing size is 33055
Total Bytes sent/received: 1024
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Total Bytes sent/received: 20480
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Total Bytes sent/received: 27648
Total Bytes sent/received: 28065