Connection Event: Carrier Detect found.390422 Iridium console active and ready... Vehicle Name: REDWING Curr Time: Tue Oct 21 05:59:13 2025 MT: 390423 DR Location: 3930.739 N -7014.139 E measured 73.303 secs ago GPS TooFar: 69696969.000 N 69696969.000 E measured 1e+308 secs ago GPS Invalid : 3932.577 N -7016.230 E measured 173.878 secs ago GPS Location: 3930.739 N -7014.139 E measured 73.543 secs ago sensor:c_autoballast_state(enum)=2 588.733 secs ago sensor:c_climb_bpump(X)=575 582.216 secs ago sensor:c_dive_bpump(X)=-625 582.22 secs ago sensor:c_iridium_current_num(enum)=0 177909 secs ago sensor:c_wpt_lat(lat)=3800 37701.4 secs ago sensor:c_wpt_lon(lon)=-6800 37701.4 secs ago sensor:m_avg_climb_rate(m/s)=-0.143250922346403 250.334 secs ago sensor:m_avg_dive_rate(m/s)=0.233403671373075 4925.5 secs ago sensor:m_battery(volts)=30.9696002233611 0.298 secs ago sensor:m_battery_amp_hours_remaining(amp-hrs)=754.80859375 0.302 secs ago sensor:m_cycle_overruns(int)=1718 64.115 secs ago sensor:m_digifin_leakdetect_reading(nodim)=952 3.31 secs ago sensor:m_dist_to_wpt(m)=256696.639674301 73.368 secs ago sensor:m_gps_dist_segment(km)=4.13783682230109 137.389 secs ago sensor:m_inflection_depth(m)=911.262586265415 4765.12 secs ago sensor:m_iridium_attempt_num(nodim)=2 40.084 secs ago sensor:m_iridium_signal_strength(nodim)=4 28.088 secs ago sensor:m_leakdetect_voltage(volts)=2.48507326007326 63.822 secs ago sensor:m_leakdetect_voltage_forward(volts)=2.48733211233211 63.786 secs ago sensor:m_leakdetect_voltage_science(volts)=2.49072039072039 63.751 secs ago sensor:m_leakdetect_voltage_stack_on(volts)=2.48583638583639 63.715 secs ago sensor:m_lithium_battery_relative_charge(%)=83.5833333333333 0.35 secs ago sensor:m_sci_cycle_overruns(int)=0 1e+308 secs ago sensor:m_system_errors(int)=0 0.16 secs ago sensor:m_tot_num_inflections(nodim)=5473 246.405 secs ago sensor:m_vacuum(inHg)=8.36541113553114 97.23 secs ago sensor:m_water_vx(m/s)=-0.094040318867216 137.44 secs ago sensor:m_water_vy(m/s)=0.082742810349248 137.444 secs ago sensor:u_alt_min_depth(m)=1200 37864.7 secs ago sensor:u_low_power_cycle_time(sec)=30 1e+308 secs ago sensor:u_use_current_correction(nodim)=2 1e+308 secs ago sensor:x_last_wpt_lat(lat)=3947.154 143675 secs ago sensor:x_last_wpt_lon(lon)=-7026.586 143675 secs ago sensor:x_surface_active(nodim)=4 588.857 secs ago ABORT HISTORY: total since reset: 3 ABORT HISTORY: last abort cause: MS_ABORT_BEH_ERROR ABORT HISTORY: last abort details: layered_control(): Behavior yo_9 entered B_ERROR state ABORT HISTORY: last abort time: 2025-10-16T17:05:54 ABORT HISTORY: last abort segment: REDWING-2025-288-0-2 (0122.0002) ABORT HISTORY: last abort mission: redwing.mi 390422 No login script found for processing. I heard a character ('CR'), but not the right one There were no pending chars in input buffer to drain. 390438 52 DRIVER_ODDITY:digifin:8:FIN_POS_INCORRECT GliderMIS 501> !where (null) -------------------------------- Vehicle Name: REDWING Curr Time: Tue Oct 21 05:59:41 2025 MT: 390450 DR Location: 3930.739 N -7014.139 E measured 101.009 secs ago GPS TooFar: 69696969.000 N 69696969.000 E measured 1e+308 secs ago GPS Invalid : 3932.577 N -7016.230 E measured 201.583 secs ago GPS Location: 3930.739 N -7014.139 E measured 101.249 secs ago sensor:c_autoballast_state(enum)=2 616.438 secs ago sensor:c_climb_bpump(X)=575 609.922 secs ago sensor:c_dive_bpump(X)=-625 609.925 secs ago sensor:c_iridium_current_num(enum)=0 177937 secs ago sensor:c_wpt_lat(lat)=3800 37729.1 secs ago sensor:c_wpt_lon(lon)=-6800 37729.1 secs ago sensor:m_avg_climb_rate(m/s)=-0.143250922346403 278.039 secs ago sensor:m_avg_dive_rate(m/s)=0.233403671373075 4953.21 secs ago sensor:m_battery(volts)=30.8786937003909 0.004 secs ago sensor:m_battery_amp_hours_remaining(amp-hrs)=754.80859375 0.007 secs ago sensor:m_cycle_overruns(int)=1718 91.821 secs ago sensor:m_digifin_leakdetect_reading(nodim)=952 1.014 secs ago sensor:m_dist_to_wpt(m)=256696.639674301 101.073 secs ago sensor:m_gps_dist_segment(km)=4.13783682230109 165.095 secs ago sensor:m_inflection_depth(m)=911.262586265415 4792.82 secs ago sensor:m_iridium_attempt_num(nodim)=0 0.077 secs ago sensor:m_iridium_signal_strength(nodim)=4 55.793 secs ago sensor:m_leakdetect_voltage(volts)=2.48263125763126 27.398 secs ago sensor:m_leakdetect_voltage_forward(volts)=2.48708791208791 27.362 secs ago sensor:m_leakdetect_voltage_science(volts)=2.49093406593407 27.327 secs ago sensor:m_leakdetect_voltage_stack_on(volts)=2.48598901098901 27.291 secs ago sensor:m_lithium_battery_relative_charge(%)=83.5833333333333 0.055 secs ago sensor:m_sci_cycle_overruns(int)=0 1e+308 secs ago sensor:m_system_errors(int)=0 7.86 secs ago sensor:m_tot_num_inflections(nodim)=5473 274.109 secs ago sensor:m_vacuum(inHg)=8.36541113553114 124.935 secs ago sensor:m_water_vx(m/s)=-0.094040318867216 165.144 secs ago sensor:m_water_vy(m/s)=0.082742810349248 165.148 secs ago sensor:u_alt_min_depth(m)=1200 37892.4 secs ago sensor:u_low_power_cycle_time(sec)=30 1e+308 secs ago sensor:u_use_current_correction(nodim)=2 1e+308 secs ago sensor:x_last_wpt_lat(lat)=3947.154 143702 secs ago sensor:x_last_wpt_lon(lon)=-7026.586 143702 secs ago sensor:x_surface_active(nodim)=4 616.562 secs ago -------------------------------- 390450 54 behavior surface_4: ! succeeded:where 390450 behavior surface_4: SUBSTATE 7 ->7 : After ! command, waiting for control-C to exit/resume 390454 55 DRIVER_ODDITY:digifin:8:FIN_POS_INCORRECT GliderMIS 567> not found>*< [dockzr | dockszr] [?][-v N][-nosmartdir][-f rf | irid][-cd dir][-noremove] [-archive] [-d ] ... [[-d ... ] ... ] 390486 63 DRIVER_ODDITY:digifin:8:FIN_POS_INCORRECT 390494 65 DRIVER_ODDITY:digifin:8:FIN_POS_INCORRECT GliderMIS 535> 390514 70 DRIVER_ODDITY:digifin not found>*< [dockzr | dockszr] [?][-v N][-nosmartdir][-f rf | irid][-cd dir][-noremove] [-archive] [-d ] ... [[-d ... ] ... ] :8:FIN_POS_INCORRECT