Connection Event: Carrier Detect found.106189 Iridium console active and ready... Vehicle Name: ru34 Curr Time: Mon Feb 19 06:29:26 2024 MT: 106189 DR Location: 4109.122 N -7107.705 E measured 829.714 secs ago GPS TooFar: 69696969.000 N 69696969.000 E measured 1e+308 secs ago GPS Invalid : 4110.371 N -7107.131 E measured 881.914 secs ago GPS Location: 4109.122 N -7107.705 E measured 831.421 secs ago sensor:c_wpt_lat(lat)=4108.191 12516.2 secs ago sensor:c_wpt_lon(lon)=-7107.621 12516.2 secs ago sensor:m_battery(volts)=14.2956223415291 668.575 secs ago sensor:m_coulomb_amphr(amp-hrs)=347.052053999658 3.802 secs ago sensor:m_coulomb_amphr_total(amp-hrs)=348.937041999654 3.807 secs ago sensor:m_depth(m)=0.694065878385896 3.708 secs ago sensor:m_digifin_leakdetect_reading(nodim)=1023 0.048 secs ago sensor:m_gps_mag_var(rad)=0.253072741539178 831.467 secs ago sensor:m_iridium_attempt_num(nodim)=3 36.045 secs ago sensor:m_iridium_call_num(nodim)=5438 0.059 secs ago sensor:m_iridium_dialed_num(nodim)=6816 8.063 secs ago sensor:m_leakdetect_voltage(volts)=2.49062881562882 676.703 secs ago sensor:m_leakdetect_voltage_forward(volts)=2.47967032967033 676.667 secs ago sensor:m_leakdetect_voltage_science(volts)=2.47823565323565 676.632 secs ago sensor:m_tot_num_inflections(nodim)=118649 889.898 secs ago sensor:m_vacuum(inHg)=8.13987277167277 668.579 secs ago sensor:m_water_vx(m/s)=0.101403441461232 849.889 secs ago sensor:m_water_vy(m/s)=0.011262983184958 849.892 secs ago sensor:u_max_altimeter(m)=50 1e+308 secs ago sensor:u_min_water_depth(m)=0 1e+308 secs ago sensor:u_use_current_correction(nodim)=1 1e+308 secs ago sensor:x_last_wpt_lat(lat)=4111.1696 16601.2 secs ago sensor:x_last_wpt_lon(lon)=-7107.6502 16601.2 secs ago ABORT HISTORY: total since reset: 6 ABORT HISTORY: last abort cause: MS_ABORT_BEH_ERROR ABORT HISTORY: last abort details: layered_control(): Behavior surface_3 entered B_ERROR state ABORT HISTORY: last abort time: 2024-02-18T00:54:00 ABORT HISTORY: last abort segment: ru34-2024-046-0-27 (0252.0027) ABORT HISTORY: last abort mission: 50_n.mi 106189 No login script found for processing. SCI ERROR: timed out waiting for science to stop logging106192 ERROR behavior surface_3: Error from prepare_to_start_next_logging_segment() 106192 behavior surface_3: STATE Active -> ERROR 106192 ERROR behavior surface_3: Entered B_ERROR State 106192 ERROR behavior ?_-1: layered_control(): Behavior surface_3 entered B_ERROR state 106199 ERROR behavior ?_-1: abort_the_mission(0): (6)MS_ABORT_BEH_ERROR 106199 behavior ?_-1: abort_the_mission(): Changing U_CYCLE_TIME from 4.000000 to 15.000000 106199 save_and_change_sensors().... Changed u_depth_rate_filter_factor from 4 to -1 106199 Attempting to put only critical devices back into service 106199 behavior ?_-1: Vehicle Name: ru34 106199 behavior ?_-1: abort_the_mission(): (6)MS_ABORT_BEH_ERROR 106199 behavior ?_-1: secs since abort started: 0 try num: 0 106199 behavior ?_-1: depths ini: 1 working: 51 at risk: 221 crush: 225 106199 behavior ?_-1: expected time/tries to surface: 315 20 106199 behavior ?_-1: max time/tries to go up: 300 20 106199 behavior ?_-1: too long: 0, not going up: 0, depth sensor busted:0 106199 behavior ?_-1: abort burn time/tries min: 600 40 106199 behavior ?_-1: abort burn time/tries max: 86400 5760 106199 behavior ?_-1: ABOVE WORKING DEPTH 106199 behavior ?_-1: drop_the_weight = 0 106199 Not recommended, but if in infinite loop, hit Control-C 106201 sensor: m_depth = 0.26346174159135 m 106201 49 Attempting to put only critical devices back into service 106201 behavior ?_-1: Vehicle Name: ru34 106201 behavior ?_-1: abort_the_mission(): (6)MS_ABORT_BEH_ERROR 106201 behavior ?_-1: secs since abort started: 2 try num: 1 106201 behavior ?_-1: depths ini: 1 working: 51 at risk: 221 crush: 225 106201 behavior ?_-1: expected time/tries to surface: 315 20 106201 behavior ?_-1: max time/tries to go up: 300 20 106201 behavior ?_-1: too long: 0, not going up: 0, depth sensor busted:0 106201 behavior ?_-1: abort burn time/tries min: 600 40 106201 behavior ?_-1: abort burn time/tries max: 86400 5760 106201 behavior ?_-1: ABOVE WORKING DEPTH 106201 behavior ?_-1: drop_the_weight = 0 106201 Not recommended, but if in infinite loop, hit Control-C 106203 sensor: m_depth = 0.535422249040533 m 106216 50 Attempting to put only critical devices back into service 106216 behavior ?_-1: Vehicle Name: ru34 106216 behavior ?_-1: abort_the_mission(): (6)MS_ABORT_BEH_ERROR 106216 behavior ?_-1: secs since abort started: 17 try num: 2 106216 behavior ?_-1: depths ini: 1 working: 51 at risk: 221 crush: 225 106216 behavior ?_-1: expected time/tries to surface: 315 20 106216 behavior ?_-1: max time/tries to go up: 300 20 106216 behavior ?_-1: too long: 0, not going up: 0, depth sensor busted:0 106216 behavior ?_-1: abort burn time/tries min: 600 40 106216 behavior ?_-1: abort burn time/tries max: 86400 5760 106216 ERROR behavior ?_-1: we_are_done(): At the surface, return (-2)MS_COMPLETED_ABNORMALLY 106216 behavior ?_-1: we_are_done(): Restoring U_CYCLE_TIME from 15.000000 to 4.000000 106216 restore_sensors().... Restored u_depth_rate_filter_factor from -1 to 4 106216 behavior ?_-1: ABOVE WORKING DEPTH 106216 behavior ?_-1: drop_the_weight = 0 106216 Not recommended, but if in infinite loop, hit Control-C 106217 behavior ?_-1: run_mission(): Mission completed: MS_COMPLETED_ABNORMALLY(-2) Vehicle Name: ru34 Mission Name: 50_n.mi Mission Number: ru34-2024-049-0-17 (0253.0017) post_mission_cleanup(): End of Mission timestamp: Mon Feb 19 06:30:00 2024 timestamp: Mon Feb 19 06:30:04 2024 Mission completed ABNORMALLY, ret = -3 Mission end: grun_mission() 50_n.mi ru34-2024-049-0-17 (0253.0017) SEQUENCE: 50_n.mi ru34-2024-049-0-17 (0253.0017) aborted on try 0 SEQUENCE: Forcing use of critical devices Returning to GliderDos to let iridium report in. Setting U_MAX_TIME_IN_GLIDERDOS(s) to 900 Command error: SEQUENCE: suspended GliderDos A 6 >why? ABORT HISTORY: total since reset: 7 ABORT HISTORY: last abort cause: MS_ABORT_BEH_ERROR ABORT HISTORY: last abort details: layered_control(): Behavior surface_3 entered B_ERROR state ABORT HISTORY: last abort time: 2024-02-19T06:29:30 ABORT HISTORY: last abort segment: ru34-2024-049-0-17 (0253.0017) ABORT HISTORY: last abort mission: 50_n.mi BOOT: Last reboot reason was REBOOT_POWER_DOWN - Power Down/Cold Boot Boot number : 329 CORE: Core dump present GliderDos A 6 >