Connection Event: Carrier Detect found. 44628 Iridium console active and ready... Vehicle Name: blue Curr Time: Wed Oct 27 02:34:07 2021 MT: 44627 DR Location: 4021.944 N -7058.271 E measured 44.75 secs ago GPS TooFar: 69696969.000 N 69696969.000 E measured 1e+308 secs ago GPS Invalid : 4025.086 N -7054.252 E measured 20527.4 secs ago GPS Location: 4021.944 N -7058.271 E measured 47.788 secs ago sensor:c_wpt_lat(lat)=4114.89 44515.1 secs ago sensor:c_wpt_lon(lon)=-7057.21 44515.2 secs ago sensor:m_battery(volts)=13.8729340646204 4.209 secs ago sensor:m_coulomb_amphr(amp-hrs)=162.985565185547 4.346 secs ago sensor:m_coulomb_amphr_total(amp-hrs)=163.132815685545 4.359 secs ago sensor:m_depth(m)=0 4.271 secs ago sensor:m_digifin_leakdetect_reading(nodim)=415 4.484 secs ago sensor:m_gps_mag_var(rad)=0.249582083035189 48.148 secs ago sensor:m_iridium_attempt_num(nodim)=1 40.467 secs ago sensor:m_iridium_call_num(nodim)=4635 0.497 secs ago sensor:m_iridium_dialed_num(nodim)=8291 12.73 secs ago sensor:m_leakdetect_voltage(volts)=2.470115995116 24.094 secs ago sensor:m_leakdetect_voltage_forward(volts)=2.46504884004884 24.109 secs ago sensor:m_leakdetect_voltage_science(volts)=-1 4.684 secs ago sensor:m_system_clock_lags_gps(sec)=1 48.383 secs ago sensor:m_tot_num_inflections(nodim)=6811 1e+308 secs ago sensor:m_vacuum(inHg)=9.26117524420024 4.689 secs ago sensor:m_water_vx(m/s)=-0.178389249872339 1e+308 secs ago sensor:m_water_vy(m/s)=0.095752311517572 1e+308 secs ago sensor:u_max_altimeter(m)=100 1e+308 secs ago sensor:u_min_altimeter(m)=2 1e+308 secs ago sensor:u_min_water_depth(m)=50 1e+308 secs ago sensor:u_use_current_correction(nodim)=1 1e+308 secs ago sensor:x_last_wpt_lat(lat)=4000 1e+308 secs ago sensor:x_last_wpt_lon(lon)=-7054 1e+308 secs ago ABORT HISTORY: total since reset: 3 ABORT HISTORY: last abort cause: MS_ABORT_LEAK ABORT HISTORY: last abort details: There is a leak in the digifin. ABORT HISTORY: last abort time: 2021-10-21T11:59:29 ABORT HISTORY: last abort segment: blue-2021-293-0-0 (0114.0000) ABORT HISTORY: last abort mission: 100_NW.MI 44629 No login script found for processing. this is a long expression that delays to get whole surface dialog Bad command or file name GliderDos N -1 > GliderDos N -1 > GliderDos N -1 >put c_gps_on 0 44654 35 sensor: c_gps_on = 0 enum GliderDos N -1 > GliderDos N -1 > GliderDos N -1 > GliderDos N -1 >callback 3 I am going to hangup the Iridium! I will call you back in 3 minutes at the primary number ( 88160000592 ) GliderDos N -1 > 44664 42 disabling Iridium conso