Connection Event: Carrier Detect found. NO CARRIER RING CONNECT 4800/ARQ/V32/LAPM 70029 Iridium console active and ready... Vehicle Name: maracoos_01 Curr Time: Mon Oct 26 03:09:25 2020 MT: 70029 DR Location: 3826.381 N -7430.850 E measured 208.152 secs ago GPS TooFar: 69696969.000 N 69696969.000 E measured 1e+308 secs ago GPS Invalid : 3826.757 N -7431.789 E measured 305.844 secs ago GPS Location: 3826.381 N -7430.850 E measured 210.855 secs ago sensor:c_autoballast_state(enum)=2 1139.78 secs ago sensor:c_climb_bpump(X)=207.5 738.745 secs ago sensor:c_dive_bpump(X)=-92.5 738.749 secs ago sensor:c_iridium_current_num(enum)=1 1e+308 secs ago sensor:c_wpt_lat(lat)=3829.018 69978.2 secs ago sensor:c_wpt_lon(lon)=-7427.591 69978.2 secs ago sensor:m_battery(volts)=14.2668559097477 179.239 secs ago sensor:m_bms_aft_current(amp)=0.11125 3.913 secs ago sensor:m_bms_ebay_current(amp)=-0.000625 3.943 secs ago sensor:m_bms_pitch_current(amp)=0.156876 3.975 secs ago sensor:m_coulomb_amphr(amp-hrs)=96.8336080000039 3.832 secs ago sensor:m_coulomb_amphr_total(amp-hrs)=97.1923500000026 3.836 secs ago sensor:m_digifin_leakdetect_reading(nodim)=1022 0.198 secs ago sensor:m_iridium_attempt_num(nodim)=1 44.066 secs ago sensor:m_iridium_signal_strength(nodim)=3 28.196 secs ago sensor:m_leakdetect_voltage(volts)=2.49746642246642 171.221 secs ago sensor:m_leakdetect_voltage_forward(volts)=2.49777167277167 171.185 secs ago sensor:m_leakdetect_voltage_science(volts)=2.49880952380952 171.15 secs ago sensor:m_lithium_battery_relative_charge(%)=54.7942558139523 3.867 secs ago sensor:m_tot_num_inflections(nodim)=12611 417.175 secs ago sensor:m_vacuum(inHg)=8.49310461538461 151.128 secs ago sensor:m_water_vx(m/s)=-0.090976417183648 272.804 secs ago sensor:m_water_vy(m/s)=-0.279141785867421 272.807 secs ago sensor:u_alt_min_depth(m)=2 1e+308 secs ago sensor:u_use_current_correction(nodim)=1 1e+308 secs ago sensor:x_last_wpt_lat(lat)=3847.057 1e+308 secs ago sensor:x_last_wpt_lon(lon)=-7509.6052 1e+308 secs ago ABORT HISTORY: total since reset: 17 ABORT HISTORY: last abort cause: MS_ABORT_BEH_ERROR ABORT HISTORY: last abort details: layered_control(): Behavior surface_2 entered B_ERROR state ABORT HISTORY: last abort time: 2020-10-25T07:19:52 ABORT HISTORY: last abort segment: maracoos_01-2020-298-0-4 (0060.0004) ABORT HISTORY: last abort mission: a100.mi 70029 No login script found for processing. :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:-0.0608 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:0.0695 C_FIN:0.0000 70105 39 SCI ERROR: science start logging failed GLD: ERROR resuming logging -------------------------------- Error from CmdDispatch():Error sending files 70105 ERROR behavior surface_2: S COMMAND FAILED: s *.sbd *.tbd *.vem *.azf *.asc Glider maracoos_01 at surface. Because:no comms for a while [behavior surface_2 start_when = 12.0] MissionName:a100.mi MissionNum:maracoos_01-2020-298-1-11 (0061.0011) Vehicle Name: maracoos_01 Curr Time: Mon Oct 26 03:10:42 2020 MT: 70106 DR Location: 3826.381 N -7430.850 E measured 284.848 secs ago GPS TooFar: 69696969.000 N 69696969.000 E measured 1e+308 secs ago GPS Invalid : 3826.757 N -7431.789 E measured 382.539 secs ago GPS Location: 3826.381 N -7430.850 E measured 287.551 secs ago sensor:c_autoballast_state(enum)=2 1216.47 secs ago sensor:c_climb_bpump(X)=207.5 815.441 secs ago sensor:c_dive_bpump(X)=-92.5 815.445 secs ago sensor:c_iridium_current_num(enum)=1 1e+308 secs ago sensor:c_wpt_lat(lat)=3829.018 70054.9 secs ago sensor:c_wpt_lon(lon)=-7427.591 70054.9 secs ago sensor:m_battery(volts)=14.2633419915446 0.276 secs ago sensor:m_bms_aft_current(amp)=0.102812 0.465 secs ago sensor:m_bms_ebay_current(amp)=-0.000625 0.496 secs ago sensor:m_bms_pitch_current(amp)=0.160312 0.528 secs ago sensor:m_coulomb_amphr(amp-hrs)=96.8398320000039 0.385 secs ago sensor:m_coulomb_amphr_total(amp-hrs)=97.1985740000027 0.389 secs ago sensor:m_digifin_leakdetect_reading(nodim)=1023 0.615 secs ago sensor:m_iridium_attempt_num(nodim)=1 120.762 secs ago sensor:m_iridium_signal_strength(nodim)=3 104.892 secs ago sensor:m_leakdetect_voltage(volts)=2.49697802197802 0.173 secs ago sensor:m_leakdetect_voltage_forward(volts)=2.49746642246642 0.137 secs ago sensor:m_leakdetect_voltage_science(volts)=2.49874847374847 0.102 secs ago sensor:m_lithium_battery_relative_charge(%)=54.7913609302313 0.42 secs ago sensor:m_tot_num_inflections(nodim)=12611 493.871 secs ago sensor:m_vacuum(inHg)=8.57315648351648 0.286 secs ago sensor:m_water_vx(m/s)=-0.090976417183648 349.5 secs ago sensor:m_water_vy(m/s)=-0.279141785867421 349.502 secs ago sensor:u_alt_min_depth(m)=2 1e+308 secs ago sensor:u_use_current_correction(nodim)=1 1e+308 secs ago sensor:x_last_wpt_lat(lat)=3847.057 1e+308 secs ago sensor:x_last_wpt_lon(lon)=-7509.6052 1e+308 secs ago devices:(t/m/s) errs: 0/ 0/ 0 warn: 100/ 6/ 1 odd: 717/ 30/ 5 ABORT HISTORY: total since reset: 17 ABORT HISTORY: last abort cause: MS_ABORT_BEH_ERROR ABORT HISTORY: last abort details: layered_control(): Behavior surface_2 entered B_ERROR state ABORT HISTORY: last abort time: 2020-10-25T07:19:52 ABORT HISTORY: last abort segment: maracoos_01-2020-298-0-4 (0060.0004) ABORT HISTORY: last abort mission: a100.mi Hit Control-R to RESUME the mission, i.e. dive! Hit Control-C to END the mission, i.e. GliderDos Hit Control-E to extend surface time by 5 minutes. Hit Control-W to get device warning reports. Hit Control-F to re-read yo, goto_l, surface, sample, drift_ mafiles. Hit H <0:1> to Hangup and call back in minutes at 0-primary 1-alternate number. Hit S [-f={rf}|{irid] [-num=] [-t=] [filespec ...] to send log files Hit ! to execute Hit Control-T to consci to science computer when comms ready: ... communications NOT ready for consci. ... because: m_science_clothesline_lag not updated this cycle Water Velocity Calculations waiting for final gps fix(ideally -209 secs) Waypoint: (3829.0180,-7427.5910) Range: 6800m, Bearing: 56deg, Age: 19:27h:m Time until diving is: 11 secs :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:-0.0695 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:0.0666 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:-0.0318 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:0.0695 C_FIN:0.0000 70186 60 SCI:PROGLET house_elf begin() called 70186 SCI: house_elf: Version 1.2 70186 SCI:PROGLET ctd41cp begin() called 70186 SCI: ctd41cp: Version 0.2 70186 SCI: ctd41cp: Will be sending the following data to glider: 70186 SCI: sci_water_cond(s/m) 70186 SCI: sci_water_temp(degc) 70186 SCI: sci_water_pressure(bar) 70186 SCI: sci_ctd41cp_timestamp(timestamp) 70186 SCI:PROGLET flbbcd begin() called 70186 SCI: flbbcd: Version 0.0 70186 SCI: flbbcd: Will be sending following data to glider: 70186 SCI: sci_flbbcd_chlor_units(ug/l) 70186 SCI: sci_flbbcd_bb_units(nodim) 70186 SCI: sci_flbbcd_cdom_units(ppb) 70186 SCI: sci_flbbcd_chlor_sig(nodim) 70186 SCI: sci_flbbcd_bb_sig(nodim) 70186 SCI: sci_flbbcd_cdom_sig(nodim) 70186 SCI: sci_flbbcd_chlor_ref(nodim) 70186 SCI: sci_flbbcd_bb_ref(nodim) 70186 SCI: sci_flbbcd_cdom_ref(nodim) 70186 SCI: sci_flbbcd_therm(nodim) 70186 SCI: sci_flbbcd_timestamp(timestamp) 70186 SCI:Bit(0) raise count is now 0. 70186 SCI:Bit(0) raise count is now 0. 70186 SCI:PROGLET house_elf start() called 70186 SCI: house_elf_run(): 0 error(s) in a row. (5 is fatal) 70186 SCI: house_elf_run(): 0 error(s) since house_elf_begin(). (50 is fatal) :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:-0.0782 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:0.0753 C_FIN:0.0000 SCI ERROR: timed out waiting for science to stop logging 70241 73 ERROR behavior surface_2: Error from prepare_to_start_next_logging_segment() 70241 behavior surface_2: STATE Active -> ERROR 70241 ERROR behavior surface_2: Entered B_ERROR State ^W 70241 ERROR behavior ?_-1: layered_control(): Behavior surface_2 entered B_ERROR state 70245 ERROR behavior ?_-1: abort_the_mission(0): (6)MS_ABORT_BEH_ERROR 70245 behavior ?_-1: abort_the_mission(): Changing U_CYCLE_TIME from 4.000000 to 15.000000 70245 save_and_change_sensors().... Changed u_depth_rate_filter_factor from 4 to -1 70245 Attempting to put only critical devices back into service 70245 behavior ?_-1: Vehicle Name: maracoos_01 70245 behavior ?_-1: abort_the_mission(): (6)MS_ABORT_BEH_ERROR 70245 behavior ?_-1: secs since abort started: 0 try num: 0 70245 behavior ?_-1: depths ini: 0 working: 102 at risk: 221 crush: 225 70245 behavior ?_-1: expected time/tries to surface: 300 20 70245 behavior ?_-1: max time/tries to go up: 300 20 70245 behavior ?_-1: too long: 0, not going up: 0, depth sensor busted:0 70245 behavior ?_-1: abort burn time/tries min: 600 40 70245 behavior ?_-1: abort burn time/tries max: 14400 960 70245 behavior ?_-1: ABOVE WORKING DEPTH 70245 behavior ?_-1: drop_the_weight = 0 70245 Not recommended, but if in infinite loop, hit Control-C 70250 sensor: m_depth = 0 m 70250 74 Attempting to put only critical devices back into service 70250 behavior ?_-1: Vehicle Name: maracoos_01 70250 behavior ?_-1: abort_the_mission(): (6)MS_ABORT_BEH_ERROR 70250 behavior ?_-1: secs since abort started: 5 try num: 1 70250 behavior ?_-1: depths ini: 0 working: 102 at risk: 221 crush: 225 70250 behavior ?_-1: expected time/tries to surface: 300 20 70250 behavior ?_-1: max time/tries to go up: 300 20 70250 behavior ?_-1: too long: 0, not going up: 0, depth sensor busted:0 70250 behavior ?_-1: abort burn time/tries min: 600 40 70250 behavior ?_-1: abort burn time/tries max: 14400 960 70250 behavior ?_-1: ABOVE WORKING DEPTH 70250 behavior ?_-1: drop_the_weight = 0 70250 Not recommended, but if in infinite loop, hit Control-C 70252 sensor: m_depth = 0.671286100309323 m 70265 75 Attempting to put only critical devices back into service 70265 behavior ?_-1: Vehicle Name: maracoos_01 70265 behavior ?_-1: abort_the_mission(): (6)MS_ABORT_BEH_ERROR 70265 behavior ?_-1: secs since abort started: 20 try num: 2 70265 behavior ?_-1: depths ini: 0 working: 102 at risk: 221 crush: 225 70265 behavior ?_-1: expected time/tries to surface: 300 20 70265 behavior ?_-1: max time/tries to go up: 300 20 70265 behavior ?_-1: too long: 0, not going up: 0, depth sensor busted:0 70265 behavior ?_-1: abort burn time/tries min: 600 40 70265 behavior ?_-1: abort burn time/tries max: 14400 960 70265 ERROR behavior ?_-1: we_are_done(): At the surface, return (-2)MS_COMPLETED_ABNORMALLY 70265 behavior ?_-1: we_are_done(): Restoring U_CYCLE_TIME from 15.000000 to 4.000000 70265 restore_sensors().... Restored u_depth_rate_filter_factor from -1 to 4 70265 behavior ?_-1: ABOVE WORKING DEPTH 70265 behavior ?_-1: drop_the_weight = 0 70265 Not recommended, but if in infinite loop, hit Control-C 70266 behavior ?_-1: run_mission(): Mission completed: MS_COMPLETED_ABNORMALLY(-2) Vehicle Name: maracoos_01 Mission Name: a100.mi Mission Number: maracoos_01-2020-298-1-11 (0061.0011) post_mission_cleanup(): End of Mission timestamp: Mon Oct 26 03:13:26 2020 timestamp: Mon Oct 26 03:13:30 2020 Mission completed ABNORMALLY, ret = -3 Mission end: grun_mission() a100.mi maracoos_01-2020-298-1-11 (0061.0011) SEQUENCE: a100.mi maracoos_01-2020-298-1-11 (0061.0011) aborted on try 0 SEQUENCE: Forcing use of critical devices Returning to GliderDos to let iridium report in. Setting U_MAX_TIME_IN_GLIDERDOS(s) to 900 Command error: SEQUENCE: suspended GliderDos A 6 > Vehicle Name: maracoos_01 70274 76 GliderDos: No keystroke heard for 0 seconds 900 seconds to go before running:SEQUENCE -resume_next GliderDos A 6 >why? ABORT HISTORY: total since reset: 18 ABORT HISTORY: last abort cause: MS_ABORT_BEH_ERROR ABORT HISTORY: last abort details: layered_control(): Behavior surface_2 entered B_ERROR state ABORT HISTORY: last abort time: 2020-10-26T03:12:57 ABORT HISTORY: last abort segment: maracoos_01-2020-298-1-11 (0061.0011) ABORT HISTORY: last abort mission: a100.mi BOOT: Last reboot reason was REBOOT_BROWN_OUT - Power Brown Out/Cold Boot Boot number : 204 CORE: Core dump present GliderDos A 6 > GliderDos A 6 > GliderDos A 6 >:OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:-0.0753 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:0.0695 C_FIN:0.0000 GliderDos A 6 >:OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:-0.0724 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:0.0376 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:-0.0753 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:0.0724 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:-0.0695 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:0.0753 C_FIN:0.0000 GliderDos A 6 >:OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:-0.0637 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:0.0840 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:-0.0434 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:0.0724 C_FIN:0.0000 Vehicle Name: maracoos_01 70586 53 GliderDos: No keystroke heard for 300 seconds 600 seconds to go before running:SEQUENCE -resume_next GliderDos A 6 >:OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:-0.0753 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:0.0289 C_FIN:0.0000 GliderDos A 6 >:OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:-0.0637 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:0.0550 C_FIN:0.0000 Vehicle Name: maracoos_01 70711 82 NOTE:GPS fix is getting stale: 892 secs old GliderDos A 6 > GliderDos A 6 >:OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:-0.0695 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:0.0811 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:-0.0376 C_FIN:0.0000 Vehicle Name: maracoos_01 70835 12 GliderDos: No keystroke heard for 540 seconds 360 seconds to go before running:SEQUENCE -resume_next GliderDos A 6 >:OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:0.0405 C_FIN:0.0000 GliderDos A 6 > Vehicle Name: maracoos_01 70959 42 GliderDos: No keystroke heard for 660 seconds 240 seconds to go before running:SEQUENCE -resume_next GliderDos A 6 >:OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:-0.0608 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:0.0666 C_FIN:0.0000 Vehicle Name: maracoos_01 71020 57 NOTE:GPS fix is getting stale: 1202 secs old GliderDos A 6 >:OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:-0.0724 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:0.0724 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:-0.0782 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:0.0811 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:-0.0695 C_FIN:0.0000 Vehicle Name: maracoos_01 71083 72 GliderDos: No keystroke heard for 780 seconds 120 seconds to go before running:SEQUENCE -resume_next GliderDos A 6 >:OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:0.0724 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:-0.0608 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:0.0579 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:-0.0318 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:0.0579 C_FIN:0.0000 Vehicle Name: maracoos_01 71143 87 GliderDos: No keystroke heard for 840 seconds 60 seconds to go before running:SEQUENCE -resume_next GliderDos A 6 > Vehicle Name: maracoos_01 71177 95 GliderDos: No keystroke heard for 870 seconds 30 seconds to go before running:SEQUENCE -resume_next GliderDos A 6 > GliderDos: AUTOEXECUTING:SEQUENCE -resume_next SEQUENCE a100.mi(3) Sequencing missions load_mission(): Opening Mission file: a100.mi for execution 3 times Validated SENSOR c_science_all_on_enabled(bool) value 0.000000 Validated SENSOR u_use_ctd_depth_for_flying(bool) value 0.000000 Validated SENSOR u_use_current_correction(nodim) value 1.000000 load_mission(): Opening Mission file: lastgasp.mi for execution FOREVER Validated SENSOR u_pitch_motor_test_availability(bool) value 0.000000 1 mission specifiers - sequencing 3 total missions (not counting lastgasp.mi): a100.mi(3) lastgasp.mi ABORT HISTORY: total since reset: 18 ABORT HISTORY: last abort cause: MS_ABORT_BEH_ERROR ABORT HISTORY: last abort details: layered_control(): Behavior surface_2 entered B_ERROR state ABORT HISTORY: last abort time: 2020-10-26T03:12:57 ABORT HISTORY: last abort segment: maracoos_01-2020-298-1-11 (0061.0011) ABORT HISTORY: last abort mission: a100.mi Vehicle Name: maracoos_01 SEQUENCE: About to run a100.mi on try 0 You have 120 seconds to type a control-C to terminate the sequence. The control-P character immediately starts the mission. All other characters are ignored. :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:-0.0434 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:-0.0666 C_FIN:0.0000 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:0.0261 C_FIN:0.0000 I heard NO chars, starting the sequence SEQUENCE: Running a100.mi on try 0 Starting Mission: a100.mi timestamp: Mon Oct 26 03:31:09 2020 load_mission(): Opening Mission file: a100.mi Setting SENSOR c_science_all_on_enabled(bool) value 0.000000 Setting SENSOR u_use_ctd_depth_for_flying(bool) value 0.000000 Setting SENSOR u_use_current_correction(nodim) value 1.000000 Vehicle Name: maracoos_01 Curr Time: Mon Oct 26 03:31:09 2020 MT: 71325 DR Location: 3826.209 N -7430.869 E measured 0.474 secs ago GPS TooFar: 69696969.000 N 69696969.000 E measured 1e+308 secs ago GPS Invalid : 3826.757 N -7431.789 E measured 1609.64 secs ago GPS Location: 3826.381 N -7430.850 E measured not found>yo*.ma< not found>goto_l*.ma< not found>sample*.ma< not found>surfac*.ma< [dockzr | dockszr] [?][-v N][-nosmartdir][-f rf | irid][-cd dir][-noremove] [-archive] [-d ] ... [[-d ... ] ... ] 1514.65 secs ago sensor:c_autoballast_state(enum)=2 2443.57 secs ago sensor:c_climb_bpump(X)=207.5 2042.54 secs ago sensor:c_dive_bpump(X)=-92.5 2042.54 secs ago sensor:c_iridium_current_num(enum)=1 1e+308 secs ago sensor:c_wpt_lat(lat)=3829.018 71282 secs ago sensor:c_wpt_lon(lon)=-7427.591 71282 secs ago sensor:m_battery(volts)=14.2557182752076 7.319 secs ago sensor:m_bms_aft_current(amp)=0.126874 7.507 secs ago sensor:m_bms_ebay_current(amp)=-0.000625 7.538 secs ago sensor:m_bms_pitch_current(amp)=0.1962 not found>*.dat< not found>*.ini< not found>*.cfg< [dockzr | dockszr] [?][-v N][-nosmartdir][-f rf | irid][-cd dir][-noremove] [-archive] [-d ] ... [[-d ... ] ... ] 52 7.569 secs ago sensor:m_coulomb_amphr(amp-hrs)=96.953592000004 7.426 secs ago sensor:m_coulomb_amphr_total(amp-hrs)=97.3123340000027 7.431 secs ago sensor:m_digifin_leakdetect_reading(nodim)=1022 7.657 secs ago sensor:m_iridium_attempt_num(nodim)=0 1051.72 secs ago sensor:m_iridium_signal_strength(nodim)=3 1331.99 secs ago sensor:m_leakdetect_voltage(volts)=2.4985347985348 11.627 secs ago sensor:m_leakdetect_voltage_forward(volts)=2.49783272283272 11.176 secs ago sensor:m_leakdetect_voltage_science(volts)=2.49935897435897 11.141 secs ago sensor:m_lithium_battery_relative_charge(%)=54.7384493023243 7.461 secs ago sensor:m_tot_num_inflections(nodim)=12611 1720.97 secs ago sensor:m_vacuum(inHg)=8.7717789010989 7.328 secs ago sensor:m_water_vx(m/s)=-0.090725252174994 1083.07 secs ago sensor:m_water_vy(m/s)=-0.278681048474324 1083.08 secs ago sensor:u_alt_min_depth(m)=2 1e+308 secs ago sensor:u_use_current_correction(nodim)=1 0.381 secs ago sensor:x_last_wpt_lat(lat)=3847.057 1e+308 secs ago sensor:x_last_wpt_lon(lon)=-7509.6052 1e+308 secs ago start_alldevices() PARSED iridium_phone_data for datum# 0: =========== predial initialization cmds (from c:/config/iridinit.0): ATE AT+cbst=6,0,1 AT+CSQ dial string: ATD0088160000548 from sensors: C_IRIDIUM_LEAD_ZEROS C_IRIDIUM_PHONE_NUM Iridium login script (from c:/config/loginexp.0): empty or non-existent PARSED iridium_phone_data for datum# 1: =========== predial initialization cmds (from c:/config/iridinit.1): ATE AT+cbst=6,0,1 AT+CSQ dial string: ATD0017818711614 from sensors: C_IRIDIUM_LEAD_ZEROS_ALT C_IRIDIUM_PHONE_NUM_ALT Iridium login script (from c:/config/loginexp.1): empty or non-existent PARSED iridium_phone_data for datum# 2: =========== predial initialization cmds (from c:/config/iridinit.2): ATE AT+cbst=6,0,1 dial string: ATD0017818711051 from sensors: F_IRIDIUM_LEAD_ZEROS_FACTORY F_IRIDIUM_PHONE_NUM_FACTORY Iridium login script (from c:/config/loginexp.2): empty or non-existent Running algorithm to free disk space if required Not necessary to delete any files at this time Scanning free space... Megabytes used on d: = 350.574219 Megabytes available on d: = 7524.425781 Megabytes used on w: = 0.021973 Megabytes available on w: = 0.978027 :OOD:digifin_mgr_ctrl:OUT OF DEADBAND: M_FIN:-0.0637 C_FIN:0.0000 25.22 3 00620000.mlg LOG FILE OPENED MissionSTARTDate: 26 Oct 2020 03:31:09 Z Mission Name: a100.mi Mission Number: maracoos_01-2020-299-0-0 (0062.0000) log_c_stack(): 1-abend 2-surface 3-surface 4-surface 5-surface 6-surface 7-surface 8-goto_list 9-yo 10-sample 11-sample 12-prepare_to_dive 13-sensors_in report_heap_size(): M_FREE_HEAP=172.0K(176096 bytes) M_MIN_FREE_HEAP=153.0K(156668 bytes) M_SRAM_FREE_HEAP=1399.4K(1433016 bytes) M_SRAM_MIN_FREE_HEAP=1373.2K(1406176 bytes) pre_mission_init():End of Initialization 29.30 4 behavior sensors_in_13: STATE UnInited -> Active 29.32 behavior prepare_to_dive_12: STATE UnInited -> Waiting for Activation 29.32 behavior prepare_to_dive_12: STATE Waiting for Activation -> Active 29.33 init_gps_input() 29.33 behavior prepare_to_dive_12: SUBSTATE 0 UnInited->1 : Waiting for initial GPS fix 29.34 behavior sample_11: sample(): reading bargs 29.34 behavior sample_11: Reading b_args from sample48.ma 29.35 behavior sample_11: sensor_type(enum)=48.000000 29.35 behavior sample_11: sample_time_after_state_change(s)=0.000000 29.36 behavior sample_11: intersample_time(sec)=0.000000 29.36 behavior sample_11: state_to_sample(enum)=7.000000 29.37 behavior sample_11: nth_yo_to_sample(nodim)=1.000000 29.37 behavior sample_11: intersample_depth(m)=-1.000000 29.37 behavior sample_11: min_depth(m)=-5.000000 29.38 behavior sample_11: max_depth(m)=2000.000000 29.44 behavior sample_11: STATE UnInited -> Active 29.45 behavior sample_11: SUB NO CARRIER