Connection Event: Carrier Detect found.346345 Iridium console active and ready...
Vehicle Name: ru28
Curr Time: Mon Aug 5 09:39:11 2019 MT: 346344
DR Location: 3909.549 N -7408.418 E measured 38.633 secs ago
GPS TooFar: 3908.984 N -7407.320 E measured 23885.9 secs ago
GPS Invalid : 3909.558 N -7407.647 E measured 93.646 secs ago
GPS Location: 3909.549 N -7408.418 E measured 41.007 secs ago
sensor:c_wpt_lat(lat)=3913.525 32819.4 secs ago
sensor:c_wpt_lon(lon)=-7418.315 32819.
not found>yo*.ma<
not found>goto_l*.ma<
not found>sample*.ma<
not found>surfac*.ma<
[dockzr | dockszr] [?][-v N][-nosmartdir][-f rf | irid][-cd dir][-noremove] [-archive]
[-d ] ...
[[-d ... ] ... ]
5 secs ago
sensor:m_battery(volts)=10.9428275148508 22.889 secs ago
sensor:m_coulomb_amphr(amp-hrs)=145.374938964844 5.216 secs ago
sensor:m_coulomb_amphr_total(amp-hrs)=148.445815452088 5.242 secs ago
sensor:m_depth(m)=0.0609093311966866 5.171 secs ago
sensor:m_digifin_leakdetect_reading(nodim)=1022 0.738 secs ago
sensor:m_gps_mag_var(rad)=0.218166156499291 41.601 secs ago
sensor:m_iridium_attempt_num(nodim)=1 36.737 secs ago
sensor:m_iridium_call_num(nodim)=7114 0.811 secs ago
sensor:m_iridium_dialed_num(nodim)=9936 10.225 secs ago
sensor:m_leakdetect_voltage(volts)=2.47884615384615 40.824 secs ago
sensor:m_leakdetect_voltage_forward(volts)=2.49136141636142 40.854 secs ago
sensor:m_leakdetect_voltage_science(volts)=-1 5.768 secs ago
sensor:m_tot_num_inflections(nodim)=241147 122.707 secs ago
sensor:m_vacuum(inHg)=7.39544026251526 23.621 secs ago
sensor:m_water_vx(m/s)=0.0124740454580429 66.681 secs ago
sensor:m_water_vy(m/s)=-0.106495622288896 66.733 secs ago
sensor:u_alt_min_depth(m)=1 1e+308 secs ago
sensor:u_min_water_depth(m)=0 1e+308 secs ago
sensor:u_use_current_correction(nodim)=1 1e+308 secs ago
sensor:x_last_wpt_lat(lat)=3907.273 49559.3 secs ago
sensor:x_last_wpt_lon(lon)=-7403.526 49559.4 secs ago
ABORT HISTORY: total since reset: 4
ABORT HISTORY: last abort cause: MS_ABORT_DEVICE_ERROR
ABORT HISTORY: last abort details: The science_super device driver returned an error.
ABORT HISTORY: last abort time: 2019-08-01T09:02:38
ABORT HISTORY: last abort segment: ru28-2019-211-0-22 (0425.0022)
ABORT HISTORY: last abort mission: 30_NW.MI
346347 No login script found for processing.
346347 DRIVER_ODDITY:iridium:1925:xxx_ctrl() ran too long
Glider ru28 at surface.
Because:no comms for a while [behavior surface_4 start_when = 12.0]
MissionName:30_NW.MI MissionNum:ru28-2019-212-0-92 (0426.0092)
Vehicle Name: ru28
Curr Time: Mon Aug 5 09:39:51 2019 MT: 346385
DR Location: 3909.549 N -7408.418 E measured 78.682 secs ago
GPS TooFar: 3908.984 N -7407.320 E measured 23925.9 secs ago
GPS Invalid : 3909.558 N -7407.647 E measured 133.689 secs ago
GPS Location: 3909.549 N -7408.418 E measured 81.049 secs ago
sensor:c_wpt_lat(lat)=3913.525 32859.4 secs ago
sensor:c_wpt_lon(lon)=-7418.315 32859.4 secs ago
sensor:m_battery(volts)=10.9428275148508 62.813 secs ago
sensor:m_coulomb_amphr(amp-hrs)=145.382064819336 4.112 secs ago
sensor:m_coulomb_amphr_total(amp-hrs)=148.45294130658 4.123 secs ago
sensor:m_depth(m)=0.033838517331467 4.054 secs ago
sensor:m_digifin_leakdetect_reading(nodim)=1022 4.26 secs ago
sensor:m_gps_mag_var(rad)=0.218166156499291 81.438 secs ago
sensor:m_iridium_attempt_num(nodim)=1 76.551 secs ago
sensor:m_iridium_call_num(nodim)=7114 40.599 secs ago
sensor:m_iridium_dialed_num(nodim)=9936 49.991 secs ago
sensor:m_leakdetect_voltage(volts)=2.47713675213675 17.599 secs ago
sensor:m_leakdetect_voltage_forward(volts)=2.49175824175824 17.615 secs ago
sensor:m_leakdetect_voltage_science(volts)=-1 4.478 secs ago
sensor:m_tot_num_inflections(nodim)=241147 162.416 secs ago
sensor:m_vacuum(inHg)=7.39544026251526 63.303 secs ago
sensor:m_water_vx(m/s)=0.0124740454580429 106.344 secs ago
sensor:m_water_vy(m/s)=-0.106495622288896 106.378 secs ago
sensor:u_alt_min_depth(m)=1 1e+308 secs ago
sensor:u_min_water_depth(m)=0 1e+308 secs ago
sensor:u_use_current_correction(nodim)=1 1e+308 secs ago
sensor:x_last_wpt_lat(lat)=3907.273 49598.8 secs ago
sensor:x_last_wpt_lon(lon)=-7403.526 49598.8 secs ago
devices:(t/m/s) errs: 2/ 0/ 0 warn: 45/ 7/ 0 odd:3035/1026/ 3
ABORT HISTORY: total since reset: 4
ABORT HISTORY: last abort cause: MS_ABORT_DEVICE_ERROR
ABORT HISTORY: last abort details: The science_super device driver returned an error.
ABORT HISTORY: last abort time: 2019-08-01T09:02:38
ABORT HISTORY: last abort segment: ru28-2019-211-0-22 (0425.0022)
ABORT HISTORY: last abort mission: 30_NW.MI
Hit Control-R to RESUME the mission, i.e. dive!
Hit Control-C to END the mission, i.e. GliderDos
Hit Control-E to extend surface time by 5 minutes.
Hit Control-W to get device warning reports.
Hit Control-F to re-read yo, goto_l, surface, sample, drift_ mafiles.
Hit H <0:1> to Hangup and call back in minutes at 0-primary 1-alternate number.
Hit S [-f={rf}|{irid] [-num=] [-t=] [filespec ...] to send log files
Hit ! to execute
Hit Control-T to consci to science computer when comms ready:
... communications ready for consci.
Water Velocity Calculations waiting for final gps fix(ideally -52 secs)
Waypoint: (3913.5250,-7418.3150) Range: 16031m, Bearing: 309deg, Age: 13:46h:m
Time until diving is: 512 secs
s *.sbd *.tbd
--------------------------------
346406 60 04260092.mlg LOG FILE CLOSED
SCIENCE DATA LOGGING: science IS running
CONSCI REQUESTED (using IRIDIUM as console)
ASKING SCIENCE COMPUTER TO SWITCH TO COMMAND MODE via IRIDIUM
SWITCHING TO SCIENCE COMMAND MODE over IRIDIUM
Normal operation resumes when:
SciDos> QUIT -or-
Lose CD (unplug freewave/hangup iridium) -or-
run longer than U_SCI_CMD_MAX_CONSCI_TIME(3600)s
346415 62 Neutering the Freewave Console
SCI: Implicitly limiting total transfer to 1800 secs, representing 180 KB total size
SCI: Enumerating and selecting files
SCI: About to send 2 files
Prechecking is not necessary for this invocation
START
**B00000000000000
�
Starting zModem transfer of 04260092.tbd to/from ru28 size is 27702
Total Bytes sent/received: 1024
Total Bytes sent/received: 2048
Total Bytes sent/received: 3072
Total Bytes sent/received: 4096
Total Bytes sent/received: 5120
Total Bytes sent/received: 6144
Total Bytes sent/received: 7168
Total Bytes sent/received: 8192
Total Bytes sent/received: 9216
Total Bytes sent/received: 10240
Total Bytes sent/received: 11264
Total Bytes sent/received: 12288
Total Bytes sent/received: 13313
Total Bytes sent/received: 13312
Total Bytes sent/received: 14336
Total Bytes sent/received: 15360
Total Bytes sent/received: 16384
Total Bytes sent/received: 17408
Total Bytes sent/received: 18432
Total Bytes sent/received: 19456
Total Bytes sent/received: 20480
Total Bytes sent/received: 21504
Total Bytes sent/received: 22528
Total Bytes sent/received: 23552
Total Bytes sent/received: 24576
Total Bytes sent/received: 25600
Total Bytes sent/received: 26625
Total Bytes sent/received: 26624
Total Bytes sent/received: 27648
Total Bytes sent/received: 27702
zModem transfer DONE for file 04260092.tbd
Starting zModem transfer of 04260091.tbd to/from ru28 size is 518
Total Bytes sent/received: 518
zModem transfer DONE for file 04260091.tbd
SHUFFLING FILES..
SCI: Sent 2 file(s):
c:\logs\04260092.TBD c:\logs\04260091.TBD
SCI: SUCCESS
346658 21 Freewave console restored
REVERTING FROM SCIENCE COMMAND MODE
SCIENCE COMMAND MODE TERMINATED because:
Science Program QUIT (cts lowered)
GLD: Enumerating and selecting files
GLD: About to send 2 files
Prechecking is not necessary for this invocation
346663 save_and_change_sensors()....
Changed u_use_ctd_depth_for_flying from 0 to 0
Changed c_science_on from 1 to 0
346663 save_and_change_sensors()....
Changed c_science_printout from 0 to 0
Waiting for motors idle
START
**B00000000000000
�
Starting zModem transfer of 04260092.sbd to/from ru28 size is 18860
Total Bytes sent/received: 1024
Total Bytes sent/received: 2048
Total Bytes sent/received: 3072
Total Bytes sent/received: 4096
Total Bytes sent/received: 5120
Total Bytes sent/received: 6144
Total Bytes sent/received: 7168
Total Bytes sent/received: 8192
Total Bytes sent/received: 9216
Total Bytes sent/received: 10240
Total Bytes sent/received: 11264
Total Bytes sent/received: 12288
Total Bytes sent/received: 13312
Total Bytes sent/received: 14336
Total Bytes sent/received: 15360
Total Bytes sent/received: 16384
Total Bytes sent/received: 17408
Total Bytes sent/received: 18432
Total Bytes sent/received: 18860
zModem transfer DONE for file 04260092.sbd
Starting zModem transfer of 04260091.sbd to/from ru28 size is 858
Total Bytes sent/received: 858
zModem transfer DONE for file 04260091.sbd
()....
346857 restore_sensors()....
Restored c_science_printout from 0 to 0
SHUFFLING FILES.**^XB0800000000022d
DEL*.*^XB0800000000022d
DEL
GLD: Sent 2 file(s):
c:\logs\04260092.SBD c:\logs\04260091.SBD
GLD: SUCCESS
346862 22 DRIVER_ODDITY:science_super:1814:science never cleared SCI_M_SCIENCE_ON
Glider-Science software version match: 8.000000
Science hardware version is 2.000000
346871 24 SCI:PROGLET house_elf begin() called
346871 SCI: house_elf: Version 1.2
346871 SCI:PROGLET ctd41cp begin() called
346872 SCI: ctd41cp: Version 0.2
346872 SCI: ctd41cp: Will be sending the following data to glider:
346872 SCI: sci_water_cond(s/m)
346872 SCI: sci_water_temp(degc)
346872 SCI: sci_water_pressure(bar)
346872 SCI: sci_ctd41cp_timestamp(timestamp)
346872 SCI:PROGLET lisst begin() called
346872 SCI:PROGLET flbbcd begin() called
346872 SCI: flbbcd: Version 0.0
346872 SCI: flbbcd: Will be sending following data to glider:
346872 SCI: sci_flbbcd_chlor_units(ug/l)
346873 SCI: sci_flbbcd_bb_units(nodim)
346873 SCI: sci_flbbcd_cdom_units(ppb)
346873 SCI: sci_flbbcd_chlor_sig(nodim)
346873 SCI: sci_flbbcd_bb_sig(nodim)
346873 SCI: sci_flbbcd_cdom_sig(nodim)
346873 SCI: sci_flbbcd_chlor_ref(nodim)
346873 SCI: sci_flbbcd_bb_ref(nodim)
346873 SCI: sci_flbbcd_cdom_ref(nodim)
346873 SCI: sci_flbbcd_therm(nodim)
346873 SCI: sci_flbbcd_timestamp(timestamp)
346873 SCI: Opening Bit(0) for output
346873 SCI:Bit(0) use count is now 1.
346874 SCI:Bit(0) raise count is now 0.
346874 SCI:Bit(0) raise count is now 0.
346874 SCI:PROGLET svs603 begin() called
346877 25 SCI:PROGLET house_elf start() called
346877 SCI: house_elf_run(): 0 error(s) in a row. (5 is fatal)
346877 SCI: house_elf_run(): 0 error(s) since house_elf_begin(). (50 is fatal)
346878 SCI:ERROR:tbdlist.dat:line26: Unknown sensor for logging:sci_oxy3835_wphase_oxygen, IGNORED
346878 SCI: sci_oxy3835_wphase_oxygen 4 7 -1 3
346878 SCI:ERROR:tbdlist.dat:line27: Unknown sensor for logging:sci_oxy3835_wphase_saturation, IGNORED
346878 SCI: sci_oxy3835_wphase_saturation 4 7 -1 3
346878 SCI:ERROR:tbdlist.dat:line28: Unknown sensor for logging:sci_oxy3835_wphase_temp, IGNORED
346878 SCI: sci_oxy3835_wphase_temp 12 7 -1 3
346879 SCI:ERROR:tbdlist.dat:line29: Unknown sensor for logging:sci_oxy3835_wphase_dphase, IGNORED
346879 25 SCI: sci_oxy3835_wphase_dphase 12 7 -1 3
346879 SCI:ERROR: Some sensor/interval/state modified when reading from TBD file
346880 SCI:ERROR:nbdlist.dat:line50: Unknown sensor for logging:sci_oxy3835_wphase_oxygen, IGNORED
346880 SCI:ERROR:nbdlist.dat:line51: Unknown sensor for logging:sci_oxy3835_wphase_saturation, IGNORED
346880 SCI:ERROR:nbdlist.dat:line52: Unknown sensor for logging:sci_oxy3835_wphase_temp, IGNORED
346881 SCI:ERROR:nbdlist.dat:line53: Unknown sensor for logging:sci_oxy3835_wphase_dphase, IGNORED
346881 SCI:ERROR:nbdlist.dat:line54: Unknown sensor for logging:sci_oxy3835_wphase_bphase, IGNORED
346881 SCI:ERROR:nbdlist.dat:line55: Unknown sensor for logging:sci_oxy3835_wphase_rphase, IGNORED
346881 SCI:ERROR:nbdlist.dat:line56: Unknown sensor for logging:sci_oxy3835_wphase_bamp, IGNORED
346881 SCI:ERROR:nbdlist.dat:line57: Unknown sensor for logging:sci_oxy3835_wphase_bpot, IGNORED
346881 SCI:ERROR:nbdlist.dat:line58: Unknown sensor for logging:sci_oxy3835_wphase_ramp, IGNORED
346882 SCI:ERROR:nbdlist.dat:line59: Unknown sensor for logging:sci_oxy3835_wphase_rawtemp, IGNORED
346882 SCI:ERROR:nbdlist.dat:line60: Unknown sensor for logging:sci_oxy3835_wphase_timestamp, IGNORED
346882 SCI:ERROR: Some sensor/interval/state modified when reading from NBD file
346934 04260093.mlg LOG FILE OPENED
--------------------------------
346935 behavior surface_4: SUBSTATE 7 ->7 : After data transmission, waiting for control-C to exit/resume
Glider ru28 at surface.
Because:no comms for a while [behavior surface_4 start_when = 12.0]
MissionName:30_NW.MI MissionNum:ru28-2019-212-0-93 (0426.0093)
Vehicle Name: ru28
Curr Time: Mon Aug 5 09:49:05 2019 MT: 346939
DR Location: 3909.549 N -7408.418 E measured 632.293 secs ago
GPS TooFar: 3908.984 N -7407.320 E measured 24479.5 secs ago
GPS Invalid : 3909.558 N -7407.647 E measured 687.299 secs ago
GPS Location: 3909.549 N -7408.418 E measured 634.658 secs ago
sensor:c_wpt_lat(lat)=3913.525 33413 secs ago
sensor:c_wpt_lon(lon)=-7418.315 33413 secs ago
sensor:m_battery(volts)=10.8955490416079 2.869 secs ago
sensor:m_coulomb_amphr(amp-hrs)=145.469940185547 3.045 secs ago
sensor:m_coulomb_amphr_total(amp-hrs)=148.540816672791 3.054 secs ago
sensor:m_depth(m)=0 2.931 secs ago
sensor:m_digifin_leakdetect_reading(nodim)=1022 3.208 secs ago
sensor:m_gps_mag_var(rad)=0.218166156499291 635.055 secs ago
sensor:m_iridium_attempt_num(nodim)=0 533.461 secs ago
sensor:m_iridium_call_num(nodim)=7114 594.215 secs ago
sensor:m_iridium_dialed_num(nodim)=9936 603.605 secs ago
sensor:m_leakdetect_voltage(volts)=2.47844932844933 2.836 secs ago
sensor:m_leakdetect_voltage_forward(volts)=2.49270451770452 2.85 secs ago
sensor:m_leakdetect_voltage_science(volts)=-1 2.88 secs ago
sensor:m_tot_num_inflections(nodim)=241147 716.033 secs ago
sensor:m_vacuum(inHg)=8.47367905982906 3.363 secs ago
sensor:m_water_vx(m/s)=0.0124740454580429 659.961 secs ago
sensor:m_water_vy(m/s)=-0.106495622288896 659.994 secs ago
sensor:u_alt_min_depth(m)=1 1e+308 secs ago
sensor:u_min_water_depth(m)=0 1e+308 secs ago
sensor:u_use_current_correction(nodim)=1 1e+308 secs ago
sensor:x_last_wpt_lat(lat)=3907.273 50152.4 secs ago
sensor:x_last_wpt_lon(lon)=-7403.526 50152.4 secs ago
devices:(t/m/s) errs: 2/ 0/ 0 warn: 45/ 7/ 0 odd:3036/1027/ 4
ABORT HISTORY: total since reset: 4
ABORT HISTORY: last abort cause: MS_ABORT_DEVICE_ERROR
ABORT HISTORY: last abort details: The science_super device driver returned an error.
ABORT HISTORY: last abort time: 2019-08-01T09:02:38
ABORT HISTORY: last abort segment: ru28-2019-211-0-22 (0425.0022)
ABORT HISTORY: last abort mission: 30_NW.MI
Hit Control-R to RESUME the mission, i.e. dive!
Hit Control-C to END the mission, i.e. GliderDos
Hit Control-E to extend surface time by 5 minutes.
Hit Control-W to get device warning reports.
Hit Control-F to re-read yo, goto_l, surface, sample, drift_ mafiles.
Hit H <0:1> to Hangup and call back in minutes at 0-primary 1-alternate number.
Hit S [-f={rf}|{irid] [-num=] [-t=] [filespec ...] to send log files
Hit ! to execute
Hit Control-T to consci to science computer when comms ready:
... communications NOT ready for consci.
... because: m_science_clothesline_lag > u_max_clothesline_lag_for_consci
Water Velocity Calculations waiting for final gps fix(ideally -606 secs)
Waypoint: (3913.5250,-7418.3150) Range: 16031m, Bearing: 309deg, Age: 13:55h:m
Time until diving is: 594 secs
^W name in ALLCAPS means CRITICAL device (* => SUPERCRITICAL)
[I Installed] [- Not_Installed]
[u In_use] [- Not_In_use] [X Out_of_Service]
name limits stats (#total/#mission/#segment)
0 simdrvr -
1 test_driver -
2 ARGOS* I u -1 20 5 0
3 WATCHDOG I u -1 -1 -1 0
4 DEADMAN I u -1 20 5 0
5 CONSOLE* I u -1 20 5 0
6 GPS I u -1 20 5 0
7 pinger -
8 attitude -
9 attitude_tcm3 -
10 attitude_rev I u 3 20 5 1 [ 1 0 0] [ 17 5 0] [ 0 0 0]
11 ocean_pressure I u 3 20 5 0
12 vacuum I u 3 20 5 0
13 battery I u 3 20 5 0
14lithium_battery -
15 air_pump I u 3 20 5 0
16 pitch_motor I u 3 20 5 0 [ 0 0 0] [ 0 0 0] [ 362 0 0]
17 science_super I u 3 20 5 1 [ 1 0 0] [ 28 2 0] [2006 894 1]
18 roll_motor -
19 fpitch_pump -
20 fin_motor -
21 digifin I u 3 20 5 0 [ 0 0 0] [ 0 0 0] [ 382 81 2]
22 altimeter I u 3 20 5 0
23 ctd -
24 IRIDIUM* I u -1 20 5 0 [ 0 0 0] [ 0 0 0] [ 286 52 1]
25 leakdetect I u 3 20 5 0
26 recovery -
27 coulomb I u 3 20 5 0
28 veh_temp I u 3 20 5 0
29 BUOYANCY_PUMP I u 3 20 3 0
30THERMAL_ACC_PRE -
31 THERMAL_ENGINE -
32 THERMAL_PUMP -
33 DE_PUMP -
34 HD_PUMP -
35 thruster_g1 -
36 thruster -
devices:(t/m/s) errs: 2/ 0/ 0 warn: 45/ 7/ 0 odd:3036/1027/ 4
^R346964 32 behavior surface_4: User typed Control-R, resuming
I heard a Control-R
RESUMING MISSION
Megabytes used on CF file system = 345.250000
Megabytes available on CF file system = 1652.718750
346968 04260093.mlg LOG FILE CLOSED
Doing system wide housekeeping.......
report_heap_size(): M_FREE_HEAP=182.0K, M_SPARE_HEAP=163.0K
Running algorithm to free disk space if required
Not necessary to delete any files at this time
Writing longterm state disk file: c:/state/longterm.sta
f_coulomb_battery_capacity(amp-hrs) 200.000000
f_ocean_pressure_min(volts) 0.158257
m_avg_climb_rate(m/s) -0.106473
m_avg_speed(m/s) 0.225004
m_avg_upward_inflection_time(sec) 35.456657
m_battery(volts) 10.895549
m_coulomb_amphr_total(amp-hrs) 148.546752
m_iridium_call_num(nodim) 7114.000000
m_iridium_dialed_num(nodim) 9936.000000
m_lat(lat) 3909.549200
m_lon(lon) -7408.418400
m_pump_stress_remaining_cycles(nodim) 24986.626032
m_pump_stress_track(nodim) 13.373968
m_tot_ballast_pumped_energy(kjoules) 10239.552714
m_tot_horz_dist(km) 7983.171182
m_tot_num_inflections(nodim) 241147.000000
s_ini_lat(deg) 4026.200000
s_ini_lon(deg) -7401.200000
s_water_depth_avg(m) 10.000000
s_water_depth_delta(m) 0.000000
s_water_depth_wavelength(m) 0.000000
x_de_avg_oil_vol_ierr_on_ascent(cc) 0.000000
x_de_avg_oil_vol_ierr_on_descent(cc) 0.000000
x_hover_ballast_deep(cc) 0.000000
x_hover_ballast_shallow(cc) 0.000000
x_hover_depth_deep(m) 0.000000
x_hover_depth_shallow(m) 0.000000
x_last_wpt_lat(lat) 3907.273000
x_last_wpt_lon(lon) -7403.526000
The instantaneous lag time between the system and gps clock is 0.0 seconds.
The average lag time between the system and gps clock is -0.8 seconds.
Housekeeping is done
346979 34 SCI:ERROR:tbdlist.dat:line26: Unknown sensor for logging:sci_oxy3835_wphase_oxygen, IGNORED
346980 SCI: sci_oxy3835_wphase_oxygen 4 7 -1 3
346980 SCI:ERROR:tbdlist.dat:line27: Unknown sensor for logging:sci_oxy3835_wphase_saturation, IGNORED
346980 SCI: sci_oxy3835_wphase_saturation 4 7 -1 3
346980 SCI:ERROR:tbdlist.dat:line28: Unknown sensor for logging:sci_oxy3835_wphase_temp, IGNORED
346980 SCI: sci_oxy3835_wphase_temp 12 7 -1 3
346980 SCI:ERROR:tbdlist.dat:line29: Unknown sensor for logging:sci_oxy3835_wphase_dphase, IGNORED
346981 SCI: sci_oxy3835_wphase_dphase 12 7 -1 3
346981 SCI:ERROR: Some sensor/interval/state modified when reading from TBD file
346981 SCI:ERROR:nbdlist.dat:line50: Unknown sensor for logging:sci_oxy3835_wphase_oxygen, IGNORED
346981 SCI:ERROR:nbdlist.dat:line51: Unknown sensor for logging:sci_oxy3835_wphase_saturation, IGNORED
346981 35 SCI:ERROR:nbdlist.dat:line52: Unknown sensor for logging:sci_oxy3835_wphase_temp, IGNORED
346982 SCI:ERROR:nbdlist.dat:line53: Unknown sensor for logging:sci_oxy3835_wphase_dphase, IGNORED
346983 SCI:ERROR:nbdlist.dat:line54: Unknown sensor for logging:sci_oxy3835_wphase_bphase, IGNORED
346983 SCI:ERROR:nbdlist.dat:line55: Unknown sensor for logging:sci_oxy3835_wphase_rphase, IGNORED
346983 SCI:ERROR:nbdlist.dat:line56: Unknown sensor for logging:sci_oxy3835_wphase_bamp, IGNORED
346983 SCI:ERROR:nbdlist.dat:line57: Unknown sensor for logging:sci_oxy3835_wphase_bpot, IGNORED
346983 SCI:ERROR:nbdlist.dat:line58: Unknown sensor for logging:sci_oxy3835_wphase_ramp, IGNORED
346984 SCI:ERROR:nbdlist.dat:line59: Unknown sensor for logging:sci_oxy3835_wphase_rawtemp, IGNORED
346984 SCI:ERROR:nbdlist.dat:line60: Unknown sensor for logging:sci_oxy3835_wphase_timestamp, IGNORED
346984 SCI:ERROR: Some sensor/interval/state modified when reading from NBD file
347040 36 04260094.mlg LOG FILE OPENED
Megabytes used on CF file system = 345.375000
Megabytes available on CF file system = 1652.593750
347043 init_gps_input()
347043 behavior surface_4: SUBSTATE 7 ->10 : Waiting for final gps fix
surface_4: Waiting for final GPS fix.
347045 disabling Iridium console...