Connection Event: Carrier Detect found.185935 Iridium console active and ready...
Vehicle Name: ru28
Curr Time: Sat Aug 3 13:05:41 2019 MT: 185934
DR Location: 3912.416 N -7415.660 E measured 42.205 secs ago
GPS TooFar: 3908.646 N -7425.174 E measured 87634.6 secs ago
GPS Invalid : 3912.427 N -7416.564 E measured 101.511 secs ago
GPS Location: 3912.416 N -7415.660 E measured 44.592 secs ago
sensor:c_wpt_lat(lat)=3907.273 24460.3 secs ago
sensor:c_wpt_lon(lon)=-7403.526 24460.4 secs ago
sensor:m_battery(volts)=10.89359569678 13.656 secs ago
sensor:m_coulomb_amphr(amp-hrs)=134.105575561523 5.109 secs ago
sensor:m_coulomb_amphr_total(amp-hrs)=137.176452048768 5.133 secs ago
sensor:m_depth(m)=0.0834683427510363 5.093 secs ago
sensor:m_digifin_leakdetect_reading(nodim)=1022 5.318 secs ago
sensor:m_gps_mag_var(rad)=0.218166156499291 45.189 secs ago
sensor:m_iridium_attempt_num(nodim)=1 40.307 secs ago
sensor:m_iridium_call_num(nodim)=7093 0.818 secs ago
sensor:m_iridium_dialed_num(nodim)=9915 14.279 secs ago
sensor:m_leakdetect_voltage(volts)=2.47689255189255 53.598 secs ago
sensor:m_leakdetect_voltage_forward(volts)=2.49093406593407 53.632 secs ago
sensor:m_leakdetect_voltage_science(volts)=-1 5.663 secs ago
sensor:m_tot_num_inflections(nodim)=240349 114.324 secs ago
sensor:m_vacuum(inHg)=7.50738400488401 14.39 secs ago
sensor:m_wa
not found>yo*.ma<
not found>goto_l*.ma<
not found>sample*.ma<
not found>surfac*.ma<
[dockzr | dockszr] [?][-v N][-nosmartdir][-f rf | irid][-cd dir][-noremove] [-archive]
[-d ] ...
[[-d ... ] ... ]
ter_vx(m/s)=-0.00399435740106517 70.274 secs ago
sensor:m_water_vy(m/s)=0.137527289967505 70.326 secs ago
sensor:u_alt_min_depth(m)=1 1e+308 secs ago
sensor:u_min_water_depth(m)=0 1e+308 secs ago
sensor:u_use_current_correction(nodim)=1 1e+308 secs ago
sensor:x_last_wpt_lat(lat)=3913.525 24461.8 secs ago
sensor:x_last_wpt_lon(lon)=-7418.315 24461.9 secs ago
ABORT HISTORY: total since reset: 4
ABORT HISTORY: last abort cause: MS_ABORT_DEVICE_ERROR
ABORT HISTORY: last abort details: The science_super device driver returned an error.
ABORT HISTORY: last abort time: 2019-08-01T09:02:38
ABORT HISTORY: last abort segment: ru28-2019-211-0-22 (0425.0022)
ABORT HISTORY: last abort mission: 30_NW.MI
185936 No login script found for processing.
185936 DRIVER_ODDITY:iridium:1932:xxx_ctrl() ran too long
Glider ru28 at surface.
Because:no comms for a while [behavior surface_4 start_when = 12.0]
MissionName:30_NW.MI MissionNum:ru28-2019-212-0-52 (0426.0052)
Vehicle Name: ru28
Curr Time: Sat Aug 3 13:06:21 2019 MT: 185975
DR Location: 3912.416 N -7415.660 E measured 82.181 secs ago
GPS TooFar: 3908.646 N -7425.174 E measured 87674.6 secs ago
GPS Invalid : 3912.427 N -7416.564 E measured 141.481 secs ago
GPS Location: 3912.416 N -7415.660 E measured 84.562 secs ago
sensor:c_wpt_lat(lat)=3907.273 24500.2 secs ago
sensor:c_wpt_lon(lon)=-7403.526 24500.3 secs ago
sensor:m_battery(volts)=10.89359569678 53.504 secs ago
sensor:m_coulomb_amphr(amp-hrs)=134.112686157226 4.131 secs ago
sensor:m_coulomb_amphr_total(amp-hrs)=137.183562644471 4.142 secs ago
sensor:m_depth(m)=0.0924919473727762 4.065 secs ago
sensor:m_digifin_leakdetect_reading(nodim)=1022 8.636 secs ago
sensor:m_gps_mag_var(rad)=0.218166156499291 84.951 secs ago
sensor:m_iridium_attempt_num(nodim)=1 80.042 secs ago
sensor:m_iridium_call_num(nodim)=7093 40.527 secs ago
sensor:m_iridium_dialed_num(nodim)=9915 53.968 secs ago
sensor:m_leakdetect_voltage(volts)=2.47625152625153 30.755 secs ago
sensor:m_leakdetect_voltage_forward(volts)=2.49020146520147 30.769 secs ago
sensor:m_leakdetect_voltage_science(volts)=-1 4.495 secs ago
sensor:m_tot_num_inflections(nodim)=240349 153.949 secs ago
sensor:m_vacuum(inHg)=7.50738400488401 53.989 secs ago
sensor:m_water_vx(m/s)=-0.00399435740106517 109.86 secs ago
sensor:m_water_vy(m/s)=0.137527289967505 109.893 secs ago
sensor:u_alt_min_depth(m)=1 1e+308 secs ago
sensor:u_min_water_depth(m)=0 1e+308 secs ago
sensor:u_use_current_correction(nodim)=1 1e+308 secs ago
sensor:x_last_wpt_lat(lat)=3913.525 24501.2 secs ago
sensor:x_last_wpt_lon(lon)=-7418.315 24501.3 secs ago
devices:(t/m/s) errs: 2/ 0/ 0 warn: 40/ 2/ 0 odd:2084/ 75/ 5
ABORT HISTORY: total since reset: 4
ABORT HISTORY: last abort cause: MS_ABORT_DEVICE_ERROR
ABORT HISTORY: last abort details: The science_super device driver returned an error.
ABORT HISTORY: last abort time: 2019-08-01T09:02:38
ABORT HISTORY: last abort segment: ru28-2019-211-0-22 (0425.0022)
ABORT HISTORY: last abort mission: 30_NW.MI
Hit Control-R to RESUME the mission, i.e. dive!
Hit Control-C to END the mission, i.e. GliderDos
Hit Control-E to extend surface time by 5 minutes.
Hit Control-W to get device warning reports.
Hit Control-F to re-read yo, goto_l, surface, sample, drift_ mafiles.
Hit H <0:1> to Hangup and call back in minutes at 0-primary 1-alternate number.
Hit S [-f={rf}|{irid] [-num=] [-t=] [filespec ...] to send log files
Hit ! to execute
Hit Control-T to consci to science computer when comms ready:
... communications ready for consci.
Water Velocity Calculations waiting for final gps fix(ideally -67 secs)
Waypoint: (3907.2730,-7403.5260) Range: 19895m, Bearing: 130deg, Age: 6:48h:m
Time until diving is: 508 secs
s *.sbd *.tbd
--------------------------------
185997 75 04260052.mlg LOG FILE CLOSED
SCIENCE DATA LOGGING: science IS running
CONSCI REQUESTED (using IRIDIUM as console)
ASKING SCIENCE COMPUTER TO SWITCH TO COMMAND MODE via IRIDIUM
SWITCHING TO SCIENCE COMMAND MODE over IRIDIUM
Normal operation resumes when:
SciDos> QUIT -or-
Lose CD (unplug freewave/hangup iridium) -or-
run longer than U_SCI_CMD_MAX_CONSCI_TIME(3600)s
186008 77 Neutering the Freewave Console
SCI: Implicitly limiting total transfer to 1800 secs, representing 180 KB total size
SCI: Enumerating and selecting files
SCI: About to send 2 files
Prechecking is not necessary for this invocation
START
**B00000000000000
�
Starting zModem transfer of 04260052.tbd to/from ru28 size is 26576
Total Bytes sent/received: 1024
Total Bytes sent/received: 2048
Total Bytes sent/received: 3072
Total Bytes sent/received: 4096
Total Bytes sent/received: 5120
Total Bytes sent/received: 6144
Total Bytes sent/received: 7168
Total Bytes sent/received: 8192
Total Bytes sent/received: 9216
Total Bytes sent/received: 10240
Total Bytes sent/received: 11264
Total Bytes sent/received: 12288
Total Bytes sent/received: 13313
Total Bytes sent/received: 13312
Total Bytes sent/received: 14336
Total Bytes sent/received: 15360
Total Bytes sent/received: 16384
Total Bytes sent/received: 17408
Total Bytes sent/received: 18432
Total Bytes sent/received: 19456
Total Bytes sent/received: 20480
Total Bytes sent/received: 21504
Total Bytes sent/received: 22528
Total Bytes sent/received: 23552
Total Bytes sent/received: 24576
Total Bytes sent/received: 25600
Total Bytes sent/received: 26576
zModem transfer DONE for file 04260052.tbd
Starting zModem transfer of 04260051.tbd to/from ru28 size is 518
Total Bytes sent/received: 518
zModem transfer DONE for file 04260051.tbd
SHUFFLING FILES..
SCI: Sent 2 file(s):
c:\logs\04260052.TBD c:\logs\04260051.TBD
SCI: SUCCESS
186220 27 Freewave console restored
REVERTING FROM SCIENCE COMMAND MODE
SCIENCE COMMAND MODE TERMINATED because:
Science Program QUIT (cts lowered)
GLD: Enumerating and selecting files
GLD: About to send 2 files
Prechecking is not necessary for this invocation
186224 save_and_change_sensors()....
Changed u_use_ctd_depth_for_flying from 0 to 0
Changed c_science_on from 1 to 0
186224 save_and_change_sensors()....
Changed c_science_printout from 0 to 0
Waiting for motors idle
START
**B00000000000000
�
Starting zModem transfer of 04260052.sbd to/from ru28 size is 18648
Total Bytes sent/received: 1024
Total Bytes sent/received: 2048
Total Bytes sent/received: 3072
Total Bytes sent/received: 4096
Total Bytes sent/received: 5120
Total Bytes sent/received: 6144
Total Bytes sent/received: 7168
Total Bytes sent/received: 8192
Total Bytes sent/received: 9216
Total Bytes sent/received: 10240
Total Bytes sent/received: 11264
Total Bytes sent/received: 12288
Total Bytes sent/received: 13312
Total Bytes sent/received: 14336
Total Bytes sent/received: 15360
Total Bytes sent/received: 16384
Total Bytes sent/received: 17408
Total Bytes sent/received: 18432
Total Bytes sent/received: 18648
zModem transfer DONE for file 04260052.sbd
Starting zModem transfer of 04260051.sbd to/from ru28 size is 870
Total Bytes sent/received: 870
zModem transfer DONE for file 04260051.sbd
86417 restore_sensors()....
Restored u_use_ctd_depth_for_flying from 0 to 0
Restored c_science_on from 0 to 1
186417 restore_sensors()....
186417 restore_sensors()....
Restored c_science_printout from 0 to 0
SHUFFLING FILES..
GLD: Sent 2 file(s):
c:\logs\04260052.SBD c:\logs\04260051.SBD
GLD: SUCCESS
Glider-Science software version match: 8.000000
Science hardware version is 2.000000
186426 30 SCI:PROGLET house_elf begin() called
186426 SCI: house_elf: Version 1.2
186426 SCI:PROGLET ctd41cp begin() called
186426 SCI: ctd41cp: Version 0.2
186427 SCI: ctd41cp: Will be sending the following data to glider:
186427 SCI: sci_water_cond(s/m)
186427 SCI: sci_water_temp(degc)
186427 SCI: sci_water_pressure(bar)
186427 SCI: sci_ctd41cp_timestamp(timestamp)
186427 SCI:PROGLET lisst begin() called
186427 SCI:PROGLET flbbcd begin() called
186427 SCI: flbbcd: Version 0.0
186427 SCI: flbbcd: Will be sending following data to glider:
186427 SCI: sci_flbbcd_chlor_units(ug/l)
186427 SCI: sci_flbbcd_bb_units(nodim)
186428 SCI: sci_flbbcd_cdom_units(ppb)
186428 SCI: sci_flbbcd_chlor_sig(nodim)
186428 SCI: sci_flbbcd_bb_sig(nodim)
186428 SCI: sci_flbbcd_cdom_sig(nodim)
186428 SCI: sci_flbbcd_chlor_ref(nodim)
186428 SCI: sci_flbbcd_bb_ref(nodim)
186428 SCI: sci_flbbcd_cdom_ref(nodim)
186428 SCI: sci_flbbcd_therm(nodim)
186428 31 SCI: sci_flbbcd_timestamp(timestamp)
186428 SCI: Opening Bit(0) for output
186428 SCI:Bit(0) use count is now 1.
186429 SCI:Bit(0) raise count is now 0.
186430 SCI:Bit(0) raise count is now 0.
186430 SCI:PROGLET svs603 begin() called
186436 31 SCI:PROGLET house_elf start() called
186436 SCI: house_elf_run(): 0 error(s) in a row. (5 is fatal)
186436 SCI: house_elf_run(): 0 error(s) since house_elf_begin(). (50 is fatal)
186436 SCI:PROGLET ctd41cp start() called
186436 SCI: Opening port 0:SBMB:J0
186436 SCI: 9600 baud, N81, line buf: 50, no input data timeout(secs): 15
186436 SCI: in queue size: 2048, out queue size: 0
186437 SCI:sci_uart_drain_input(0):
186437 SCI:
186437 SCI:sci_uart_drain_input:Drained 0 chars
186437 SCI:bit_shared_open(): bit(0) is already open.
186437 SCI:Bit(0) use count is now 2.
186437 SCI:bit_shared_raise(): Raising bit(0).
186437 SCI: ctd41cp_run(): 0 error(s) in a row. (5 is fatal)
186437 SCI: ctd41cp_run(): 0 error(s) since ctd41cp_begin(). (50 is fatal)
186442 32 SCI:ERROR:tbdlist.dat:line26: Unknown sensor for logging:sci_oxy3835_wphase_oxygen, IGNORED
186442 SCI: sci_oxy3835_wphase_oxygen 4 7 -1 3
186442 SCI:ERROR:tbdlist.dat:line27: Unknown sensor for logging:sci_oxy3835_wphase_saturation, IGNORED
186442 SCI: sci_oxy3835_wphase_saturation 4 7 -1 3
186443 SCI:ERROR:tbdlist.dat:line28: Unknown sensor for logging:sci_oxy3835_wphase_temp, IGNORED
186443 SCI: sci_oxy3835_wphase_temp 12 7 -1 3
186443 33 SCI:ERROR:tbdlist.dat:line29: Unknown sensor for logging:sci_oxy3835_wphase_dphase, IGNORED
186444 SCI: sci_oxy3835_wphase_dphase 12 7 -1 3
186444 SCI:ERROR: Some sensor/interval/state modified when reading from TBD file
186444 SCI:ERROR:nbdlist.dat:line50: Unknown sensor for logging:sci_oxy3835_wphase_oxygen, IGNORED
186445 SCI:ERROR:nbdlist.dat:line51: Unknown sensor for logging:sci_oxy3835_wphase_saturation, IGNORED
186445 SCI:ERROR:nbdlist.dat:line52: Unknown sensor for logging:sci_oxy3835_wphase_temp, IGNORED
186445 SCI:ERROR:nbdlist.dat:line53: Unknown sensor for logging:sci_oxy3835_wphase_dphase, IGNORED
186445 SCI:ERROR:nbdlist.dat:line54: Unknown sensor for logging:sci_oxy3835_wphase_bphase, IGNORED
186445 SCI:ERROR:nbdlist.dat:line55: Unknown sensor for logging:sci_oxy3835_wphase_rphase, IGNORED
186445 SCI:ERROR:nbdlist.dat:line56: Unknown sensor for logging:sci_oxy3835_wphase_bamp, IGNORED
186446 SCI:ERROR:nbdlist.dat:line57: Unknown sensor for logging:sci_oxy3835_wphase_bpot, IGNORED
186446 SCI:ERROR:nbdlist.dat:line58: Unknown sensor for logging:sci_oxy3835_wphase_ramp, IGNORED
186446 SCI:ERROR:nbdlist.dat:line59: Unknown sensor for logging:sci_oxy3835_wphase_rawtemp, IGNORED
186446 SCI:ERROR:nbdlist.dat:line60: Unknown sensor for logging:sci_oxy3835_wphase_timestamp, IGNORED
186446 SCI:ERROR: Some sensor/interval/state modified when reading from NBD file
186501 35 04260053.mlg LOG FILE OPENED
--------------------------------
186502 behavior surface_4: SUBSTATE 7 ->7 : After data transmission, waiting for control-C to exit/resume
Glider ru28 at surface.
Because:no comms for a while [behavior surface_4 start_when = 12.0]
MissionName:30_NW.MI MissionNum:ru28-2019-212-0-53 (0426.0053)
Vehicle Name: ru28
Curr Time: Sat Aug 3 13:15:13 2019 MT: 186507
DR Location: 3912.416 N -7415.660 E measured 614.339 secs ago
GPS TooFar: 3908.646 N -7425.174 E measured 88206.7 secs ago
GPS Invalid : 3912.427 N -7416.564 E measured 673.64 secs ago
GPS Location: 3912.416 N -7415.660 E measured 616.721 secs ago
sensor:c_wpt_lat(lat)=3907.273 25032.4 secs ago
sensor:c_wpt_lon(lon)=-7403.526 25032.4 secs ago
sensor:m_battery(volts)=10.8913354447947 2.749 secs ago
sensor:m_coulomb_amphr(amp-hrs)=134.194625854492 2.926 secs ago
sensor:m_coulomb_amphr_total(amp-hrs)=137.265502341737 2.935 secs ago
sensor:m_depth(m)=0.0293267150205971 2.803 secs ago
sensor:m_digifin_leakdetect_reading(nodim)=1022 3.079 secs ago
sensor:m_gps_mag_var(rad)=0.218166156499291 617.108 secs ago
sensor:m_iridium_attempt_num(nodim)=0 510.192 secs ago
sensor:m_iridium_call_num(nodim)=7093 572.682 secs ago
sensor:m_iridium_dialed_num(nodim)=9915 586.123 secs ago
sensor:m_leakdetect_voltage(volts)=2.47857142857143 2.735 secs ago
sensor:m_leakdetect_voltage_forward(volts)=2.49258241758242 2.748 secs ago
sensor:m_leakdetect_voltage_science(volts)=-1 2.777 secs ago
sensor:m_tot_num_inflections(nodim)=240349 686.104 secs ago
sensor:m_vacuum(inHg)=8.58770354090354 3.234 secs ago
sensor:m_water_vx(m/s)=-0.00399435740106517 642.015 secs ago
sensor:m_water_vy(m/s)=0.137527289967505 642.049 secs ago
sensor:u_alt_min_depth(m)=1 1e+308 secs ago
sensor:u_min_water_depth(m)=0 1e+308 secs ago
sensor:u_use_current_correction(nodim)=1 1e+308 secs ago
sensor:x_last_wpt_lat(lat)=3913.525 25033.4 secs ago
sensor:x_last_wpt_lon(lon)=-7418.315 25033.4 secs ago
devices:(t/m/s) errs: 2/ 0/ 0 warn: 40/ 2/ 0 odd:2084/ 75/ 5
ABORT HISTORY: total since reset: 4
ABORT HISTORY: last abort cause: MS_ABORT_DEVICE_ERROR
ABORT HISTORY: last abort details: The science_super device driver returned an error.
ABORT HISTORY: last abort time: 2019-08-01T09:02:38
ABORT HISTORY: last abort segment: ru28-2019-211-0-22 (0425.0022)
ABORT HISTORY: last abort mission: 30_NW.MI
Hit Control-R to RESUME the mission, i.e. dive!
Hit Control-C to END the mission, i.e. GliderDos
Hit Control-E to extend surface time by 5 minutes.
Hit Control-W to get device warning reports.
Hit Control-F to re-read yo, goto_l, surface, sample, drift_ mafiles.
Hit H <0:1> to Hangup and call back in minutes at 0-primary 1-alternate number.
Hit S [-f={rf}|{irid] [-num=] [-t=] [filespec ...] to send log files
Hit ! to execute
Hit Control-T to consci to science computer when comms ready:
... communications NOT ready for consci.
... because: m_science_clothesline_lag > u_max_clothesline_lag_for_consci
Water Velocity Calculations waiting for final gps fix(ideally -600 secs)
Waypoint: (3907.2730,-7403.5260) Range: 19895m, Bearing: 130deg, Age: 6:57h:m
Time until diving is: 593 secs
^W name in ALLCAPS means CRITICAL device (* => SUPERCRITICAL)
[I Installed] [- Not_Installed]
[u In_use] [- Not_In_use] [X Out_of_Service]
name limits stats (#total/#mission/#segment)
0 simdrvr -
1 test_driver -
2 ARGOS* I u -1 20 5 0
3 WATCHDOG I u -1 -1 -1 0
4 DEADMAN I u -1 20 5 0
5 CONSOLE* I u -1 20 5 0
6 GPS I u -1 20 5 0
7 pinger -
8 attitude -
9 attitude_tcm3 -
10 attitude_rev I u 3 20 5 1 [ 1 0 0] [ 14 2 0] [ 0 0 0]
11 ocean_pressure I u 3 20 5 0
12 vacuum I u 3 20 5 0
13 battery I u 3 20 5 0
14lithium_battery -
15 air_pump I u 3 20 5 0
16 pitch_motor I u 3 20 5 0 [ 0 0 0] [ 0 0 0] [ 362 0 0]
17 science_super I u 3 20 5 1 [ 1 0 0] [ 26 0 0] [1114 2 0]
18 roll_motor -
19 fpitch_pump -
20 fin_motor -
21 digifin I u 3 20 5 0 [ 0 0 0] [ 0 0 0] [ 345 44 2]
22 altimeter I u 3 20 5 0
23 ctd -
24 IRIDIUM* I u -1 20 5 0 [ 0 0 0] [ 0 0 0] [ 263 29 3]
25 leakdetect I u 3 20 5 0
26 recovery -
27 coulomb I u 3 20 5 0
28 veh_temp I u 3 20 5 0
29 BUOYANCY_PUMP I u 3 20 3 0
30THERMAL_ACC_PRE -
31 THERMAL_ENGINE -
32 THERMAL_PUMP -
33 DE_PUMP -
34 HD_PUMP -
35 thruster_g1 -
36 thruster -
devices:(t/m/s) errs: 2/ 0/ 0 warn: 40/ 2/ 0 odd:2084/ 75/ 5
^R186529 41 behavior surface_4: User typed Control-R, resuming
I heard a Control-R
RESUMING MISSION
Megabytes used on CF file system = 312.812500
Megabytes available on CF file system = 1685.156250
186534 04260053.mlg LOG FILE CLOSED
Doing system wide housekeeping.......
report_heap_size(): M_FREE_HEAP=182.0K, M_SPARE_HEAP=163.0K
Running algorithm to free disk space if required
Not necessary to delete any files at this time
Writing longterm state disk file: c:/state/longterm.sta
f_coulomb_battery_capacity(amp-hrs) 200.000000
f_ocean_pressure_min(volts) 0.158257
m_avg_climb_rate(m/s) -0.119959
m_avg_speed(m/s) 0.261493
m_avg_upward_inflection_time(sec) 21.402579
m_battery(volts) 10.891335
m_coulomb_amphr_total(amp-hrs) 137.271438
m_iridium_call_num(nodim) 7093.000000
m_iridium_dialed_num(nodim) 9915.000000
m_lat(lat) 3912.416400
m_lon(lon) -7415.660400
m_pump_stress_remaining_cycles(nodim) 24986.844357
m_pump_stress_track(nodim) 13.155643
m_tot_ballast_pumped_energy(kjoules) 10196.281412
m_tot_horz_dist(km) 7953.337434
m_tot_num_inflections(nodim) 240349.000000
s_ini_lat(deg) 4026.200000
s_ini_lon(deg) -7401.200000
s_water_depth_avg(m) 10.000000
s_water_depth_delta(m) 0.000000
s_water_depth_wavelength(m) 0.000000
x_de_avg_oil_vol_ierr_on_ascent(cc) 0.000000
x_de_avg_oil_vol_ierr_on_descent(cc) 0.000000
x_hover_ballast_deep(cc) 0.000000
x_hover_ballast_shallow(cc) 0.000000
x_hover_depth_deep(m) 0.000000
x_hover_depth_shallow(m) 0.000000
x_last_wpt_lat(lat) 3913.525000
x_last_wpt_lon(lon) -7418.315000
The instantaneous lag time between the system and gps clock is -1.0 seconds.
The average lag time between the system and gps clock is -0.8 seconds.
Housekeeping is done
186549 43 SCI:ERROR:tbdlist.dat:line26: Unknown sensor for logging:sci_oxy3835_wphase_oxygen, IGNORED
186549 SCI: sci_oxy3835_wphase_oxygen 4 7 -1 3
186549 SCI:ERROR:tbdlist.dat:line27: Unknown sensor for logging:sci_oxy3835_wphase_saturation, IGNORED
186549 SCI: sci_oxy3835_wphase_saturation 4 7 -1 3
186549 SCI:ERROR:tbdlist.dat:line28: Unknown sensor for logging:sci_oxy3835_wphase_temp, IGNORED
186550 SCI: sci_oxy3835_wphase_temp 12 7 -1 3
186550 SCI:ERROR:tbdlist.dat:line29: Unknown sensor for logging:sci_oxy3835_wphase_dphase, IGNORED
186550 SCI: sci_oxy3835_wphase_dphase 12 7 -1 3
186550 SCI:ERROR: Some sensor/interval/state modified when reading from TBD file
186550 SCI:ERROR:nbdlist.dat:line50: Unknown sensor for logging:sci_oxy3835_wphase_oxygen, IGNORED
186550 SCI:ERROR:nbdlist.dat:line51: Unknown sensor for logging:sci_oxy3835_wphase_saturation, IGNORED
186551 43 SCI:ERROR:nbdlist.dat:line52: Unknown sensor for logging:sci_oxy3835_wphase_temp, IGNORED
186551 SCI:ERROR:nbdlist.dat:line53: Unknown sensor for logging:sci_oxy3835_wphase_dphase, IGNORED
186552 SCI:ERROR:nbdlist.dat:line54: Unknown sensor for logging:sci_oxy3835_wphase_bphase, IGNORED
186552 SCI:ERROR:nbdlist.dat:line55: Unknown sensor for logging:sci_oxy3835_wphase_rphase, IGNORED
186552 SCI:ERROR:nbdlist.dat:line56: Unknown sensor for logging:sci_oxy3835_wphase_bamp, IGNORED
186552 SCI:ERROR:nbdlist.dat:line57: Unknown sensor for logging:sci_oxy3835_wphase_bpot, IGNORED
186553 SCI:ERROR:nbdlist.dat:line58: Unknown sensor for logging:sci_oxy3835_wphase_ramp, IGNORED
186553 SCI:ERROR:nbdlist.dat:line59: Unknown sensor for logging:sci_oxy3835_wphase_rawtemp, IGNORED
186553 SCI:ERROR:nbdlist.dat:line60: Unknown sensor for logging:sci_oxy3835_wphase_timestamp, IGNORED
186553 SCI:ERROR: Some sensor/interval/state modified when reading from NBD file
186609 44 04260054.mlg LOG FILE OPENED
Megabytes used on CF file system = 312.937500
Megabytes available on CF file system = 1685.031250
186611 init_gps_input()
186611 behavior surface_4: SUBSTATE 7 ->10 : Waiting for final gps f