Connection Event: Carrier Detect found. 84518 Iridium console active and ready... Vehicle Name: ru25d Curr Time: Thu Jan 18 00:05:32 2018 MT: 84517 DR Location: -6810.034 N -6847.970 E measured 66.087 secs ago GPS TooFar: 69696969.000 N 69696969.000 E measured 1e+308 secs ago GPS Invalid : -6810.112 N -6848.351 E measured 943.772 secs ago GPS Location: -6810.034 N -6847.970 E measured 68.397 secs ago sensor:c_thruster_surface_depth(m)=0 84409 secs ago sensor:c_wpt_lat(lat)=0 1e+308 secs ago sensor:c_wpt_lon(lon)=0 1e+308 secs ago sensor:m_battery(volts)=10.766248750643 4.133 secs ago sensor:m_coulomb_amphr(amp-hrs)=191.3512 4.496 secs ago sensor:m_coulomb_amphr_total(amp-hrs)=189.448703117463 4.387 secs ago sensor:m_depth(m)=0.224082171537941 4.243 secs ago sensor:m_digifin_leakdetect_reading(nodim)=1021 0.821 secs ago sensor:m_gps_mag_var(rad)=-0.376991118430775 69.076 secs ago sensor:m_iridium_attempt_num(nodim)=1 62.004 secs ago sensor:m_iridium_call_num(nodim)=2240 21.334 secs ago sensor:m_iridium_dialed_num(nodim)=3441 33.615 secs ago sensor:m_leakdetect_voltage(volts)=2.48797313797314 12.623 secs ago sensor:m_leakdetect_voltage_forward(volts)=-1 5.183 secs ago sensor:m_tot_num_inflections(nodim)=4297 1e+308 secs ago sensor:m_vacuum(inHg)=10.8262397435897 4.836 secs ago sensor:m_water_vx(m/s)=0.00446489819936013 70975.3 secs ago sensor:m_water_vy(m/s)=-0.390177340494307 70975.4 secs ago sensor:u_alt_min_depth(m)=2 1e+308 secs ago sensor:u_min_water_depth(m)=0 1e+308 secs ago sensor:u_use_current_correction(nodim)=1 1e+308 secs ago sensor:x_fin_deadband(rad)=0.04 69541 secs ago sensor:x_last_wpt_lat(lat)=-6809.5626 1e+308 secs ago sensor:x_last_wpt_lon(lon)=-6859.6243 1e+308 secs ago ABORT HISTORY: total since reset: 1 ABORT HISTORY: last abort cause: MS_ABORT_DEVICE_ERROR ABORT HISTORY: last abort details: The digifin device driver returned an error. ABORT HISTORY: last abort time: 2018-01-17T00:39:29 ABORT HISTORY: last abort segment: ru25d-2018-016-0-0 (0133.0000) ABORT HISTORY: last abort mission: initial.mi 84520 DRIVER_ODDITY:iridium:1961:xxx_ctrl() ran too long irid callback script delay Bad command or file name GliderDos A 16 > GliderDos A 16 >put c_gps_on 0 84533 5 sensor: c_gps_on = 0 enum GliderDos A 16 >callback 15 I am going to hangup the Iridium! I will call you back in 15 minutes at the primary number ( 88160000500 ) GliderDos A 16 > 84535 6 disabling Iridium cons