Connection Event: Carrier Detect found.360712 Iridium console active and ready... Vehicle Name: ru24 Curr Time: Tue Jan 31 03:40:50 2017 MT: 360712 DR Location: -6452.053 N -6413.068 E measured 0.931 secs ago GPS TooFar: -6455.973 N -6424.135 E measured 97318.3 secs ago GPS Invalid : -6452.048 N -6413.079 E measured 948.791 secs ago GPS Location: -6452.054 N -6413.075 E measured 68.311 secs ago sensor:c_thruster_surface_depth(m)=0 73407.3 secs ago sensor:c_wpt_lat(lat)=-6455.9708 74181 secs ago sensor:c_wpt_lon(lon)=-6424.2123 74181.1 secs ago sensor:m_battery(volts)=12.2102163938922 4.611 secs ago sensor:m_coulomb_amphr(amp-hrs)=0 1e+308 secs ago sensor:m_coulomb_amphr_total(amp-hrs)=0 1e+308 secs ago sensor:m_depth(m)=0.630856506555339 4.715 secs ago sensor:m_digifin_leakdetect_reading(nodim)=1023 4.976 secs ago sensor:m_gps_mag_var(rad)=-0.289724655831059 68.977 secs ago sensor:m_iridium_attempt_num(nodim)=1 61.385 secs ago sensor:m_iridium_call_num(nodim)=2961 21.673 secs ago sensor:m_iridium_dialed_num(nodim)=5534 32.299 secs ago sensor:m_leakdetect_voltage(volts)=0.485744810744811 21.532 secs ago sensor:m_leakdetect_voltage_forward(volts)=-1 5.274 secs ago sensor:m_pitch(rad)=-0.0432222306422534 4.883 secs ago sensor:m_tot_num_inflections(nodim)=25425 72810.7 secs ago sensor:m_vacuum(inHg)=15.4758066544566 5.366 secs ago sensor:m_water_vx(m/s)=0.09215781108745 73417.1 secs ago sensor:m_water_vy(m/s)=0.0759299983993855 73417.1 secs ago sensor:u_alt_min_depth(m)=2 1e+308 secs ago sensor:u_min_water_depth(m)=40 1e+308 secs ago sensor:u_use_current_correction(nodim)=1 1e+308 secs ago sensor:x_fin_deadband(rad)=0.035 360714 secs ago sensor:x_last_wpt_lat(lat)=-6455.9005 74182.5 secs ago sensor:x_last_wpt_lon(lon)=-6424.0098 74182.6 secs ago ABORT HISTORY: total since reset: 2 ABORT HISTORY: last abort cause: MS_ABORT_LEAK ABORT HISTORY: last abort details: There is a leak in the aft compartment. ABORT HISTORY: last abort time: 2017-01-30T07:27:57 ABORT HISTORY: last abort segment: ru24-2017-025-0-97 (0288.0097) ABORT HISTORY: last abort mission: 100S_N.MI 360714 DRIVER_ODDITY:iridium:1998:xxx_ctrl() ran too long put f_max_working_depth 30 360748 28 sensor: f_max_working_depth = 30 m GliderDos A 24 >put f_crush_depth 50 360752 30 sensor: f_crush_depth = 50 m GliderDos A 24 >get m_at_risk_depth = 46.200000 m GliderDos A 24 >callback 15 I am going to hangup the Iridium! I will call you back in 15 minutes at the primary number ( 88160000500 ) GliderDos A 24 >360816 49 disabling Iridium cons