56909 Iridium console active and ready... Vehicle Name: ru29 Curr Time: Thu Nov 20 05:25:50 2014 MT: 56900 DR Location: -2456.730 N -4438.154 E measured 58.481 secs ago GPS TooFar: -2453.952 N -4440.733 E measured 1e+308 secs ago GPS Invalid : -2456.421 N -4438.389 E measured 164.445 secs ago GPS Location: -2456.730 N -4438.154 E measured 60.866 secs ago sensor:c_thruster_surface_depth(m)=0 15118.3 secs ago sensor:c_thruster_surface_secs(s)=0 15118.4 secs ago sensor:c_wpt_lat(lat)=-2440 15628.8 secs ago sensor:c_wpt_lon(lon)=-4420 15628.8 secs ago sensor:m_battery(volts)=11.4153893985856 13.026 secs ago sensor:m_coulomb_amphr(amp-hrs)=19.4073123931885 13.204 secs ago sensor:m_coulomb_amphr_total(amp-hrs)=21.0893123932648 13.228 secs ago sensor:m_depth(m)=0 13.163 secs ago sensor:m_final_water_vx(m/s)=-0.179513337678253 15126.2 secs ago sensor:m_final_water_vy(m/s)=-0.139140604650796 15126.3 secs ago sensor:m_gps_mag_var(rad)=0.370009801422798 61.566 secs ago sensor:m_iridium_attempt_num(nodim)=1 56.264 secs ago sensor:m_iridium_call_num(nodim)=2545 0.892 secs ago sensor:m_iridium_dialed_num(nodim)=4634 27.85 secs ago sensor:m_leakdetect_voltage(volts)=2.49942002442002 60.804 secs ago sensor:m_leakdetect_voltage_forward(volts)=2.49520757020757 60.823 secs ago sensor:m_tot_num_inflections(nodim)=15572 332.325 secs ago sensor:m_vacuum(inHg)=8.73203736263736 13.691 secs ago sensor:m_water_vx(m/s)=-0.262257373397094 134.572 secs ago sensor:m_water_vy(m/s)=-0.161155863059387 134.616 secs ago sensor:sci_m_disk_free(Mbytes)=1987.28125 219.756 secs ago sensor:u_alt_min_depth(m)=2 1e+308 secs ago sensor:u_min_water_depth(m)=0 1e+308 secs ago sensor:u_use_current_correction(nodim)=0 1e+308 secs ago sensor:x_last_wpt_lat(lat)=-2330.0102 1e+308 secs ago sensor:x_last_wpt_lon(lon)=-4507.1071 1e+308 secs ago ABORT HISTORY: total since reset: 4 ABORT HISTORY: last abort cause: MS_ABORT_LEAK ABORT HISTORY: last abort details: There is a leak in the aft compartment. ABORT HISTORY: last abort time: 2014-11-19T10:12:54 ABORT HISTORY: last abort segment: ru29-2014-321-0-4 (0185.0004) ABORT HISTORY: last abort mission: 1K_N2.MI 56911 No login script found for processing. 56911 DRIVER_ODDITY:iridium:1835:xxx_ctrl() ran too long Glider ru29 at surface. Because:no comms for a while [behavior surface_2 start_when = 12.0] MissionName:1K_N2.MI MissionNum:ru29-2014-322-1-10 (0187.0010) Vehicle Name: ru29 Curr Time: Thu Nov 20 05:26:13 2014 MT: 56932 DR Location: -2456.730 N -4438.154 E measured 81.531 secs ago GPS TooFar: -2453.952 N -4440.733 E measured 1e+308 secs ago GPS Invalid : -2456.421 N -4438.389 E measured 187.495 secs ago GPS Location: -2456.730 N -4438.154 E measured 83.916 secs ago sensor:c_thruster_surface_depth(m)=0 15141.4 secs ago sensor:c_thruster_surface_secs(s)=0 15141.4 secs ago sensor:c_wpt_lat(lat)=-2440 15651.7 secs ago sensor:c_wpt_lon(lon)=-4420 15651.8 secs ago sensor:m_battery(volts)=11.4153893985856 35.961 secs ago sensor:m_coulomb_amphr(amp-hrs)=19.4108753204346 4.376 secs ago sensor:m_coulomb_amphr_total(amp-hrs)=21.0928753205109 4.388 secs ago sensor:m_depth(m)=0.0691307499501017 4.313 secs ago sensor:m_final_water_vx(m/s)=-0.179513337678253 15149.1 secs ago sensor:m_final_water_vy(m/s)=-0.139140604650796 15149.1 secs ago sensor:m_gps_mag_var(rad)=0.370009801422798 84.404 secs ago sensor:m_iridium_attempt_num(nodim)=1 79.085 secs ago sensor:m_iridium_call_num(nodim)=2545 23.696 secs ago sensor:m_iridium_dialed_num(nodim)=4634 50.64 secs ago sensor:m_leakdetect_voltage(volts)=2.49966422466422 21.703 secs ago sensor:m_leakdetect_voltage_forward(volts)=2.49478021978022 21.716 secs ago sensor:m_tot_num_inflections(nodim)=15572 355.088 secs ago sensor:m_vacuum(inHg)=8.73203736263736 36.44 secs ago sensor:m_water_vx(m/s)=-0.262257373397094 157.312 secs ago sensor:m_water_vy(m/s)=-0.161155863059387 157.344 secs ago sensor:sci_m_disk_free(Mbytes)=1987.28125 242.474 secs ago sensor:u_alt_min_depth(m)=2 1e+308 secs ago sensor:u_min_water_depth(m)=0 1e+308 secs ago sensor:u_use_current_correction(nodim)=0 1e+308 secs ago sensor:x_last_wpt_lat(lat)=-2330.0102 1e+308 secs ago sensor:x_last_wpt_lon(lon)=-4507.1071 1e+308 secs ago devices:(t/m/s) errs: 2/ 0/ 0 warn: 7/ 0/ 0 odd: 157/ 39/ 5 ABORT HISTORY: total since reset: 4 ABORT HISTORY: last abort cause: MS_ABORT_LEAK ABORT HISTORY: last abort details: There is a leak in the aft compartment. ABORT HISTORY: last abort time: 2014-11-19T10:12:54 ABORT HISTORY: last abort segment: ru29-2014-321-0-4 (0185.0004) ABORT HISTORY: last abort mission: 1K_N2.MI Hit Control-R to RESUME the mission, i.e. dive! Hit Control-C to END the mission, i.e. GliderDos Hit Control-E to extend surface time by 5 minutes. Hit Control-W to get device warning reports. Hit Control-F to re-read yo, goto_l, surface, sample, drift_ mafiles. Hit H <0:1> to Hangup and call back in minutes at 0-primary 1-alternate number. Hit S [-f={rf}|{irid] [-num=] [-t=] [filespec ...] to send log files Hit ! to execute Hit Control-T to consci to science computer when comms ready: ... communications ready for consci. Water Velocity Calculations waiting for final gps fix(ideally -43 secs) Waypoint: (-2440.0000,-4420.0000) Range: 43457m, Bearing: 66deg, Age: 4:20h:m Time until diving is: 508 secs Glider ru29 at surface. Because:no comms for a while [behavior surface_2 start_when = 12.0] MissionName:1K_N2.MI MissionNum:ru29-2014-322-1-10 (0187.0010) Vehicle Name: ru29 Curr Time: Thu Nov 20 05:26:56 2014 MT: 56975 DR Location: -2456.730 N -4438.154 E measured 124.863 secs ago GPS TooFar: -2453.952 N -4440.733 E measured 1e+308 secs ago GPS Invalid : -2456.421 N -4438.389 E measured 230.827 secs ago GPS Location: -2456.730 N -4438.154 E measured 127.247 secs ago sensor:c_thruster_surface_depth(m)=0 15184.7 secs ago sensor:c_thruster_surface_secs(s)=0 15184.7 secs ago sensor:c_wpt_lat(lat)=-2440 15695.1 secs ago sensor:c_wpt_lon(lon)=-4420 15695.1 secs ago sensor:m_battery(volts)=11.4075999092765 13.845 secs ago sensor:m_coulomb_amphr(amp-hrs)=19.4168109893799 4.55 secs ago sensor:m_coulomb_amphr_total(amp-hrs)=21.0988109894562 4.565 secs ago sensor:m_depth(m)=0.152087649890254 4.485 secs ago sensor:m_final_water_vx(m/s)=-0.179513337678253 15192.4 secs ago sensor:m_final_water_vy(m/s)=-0.139140604650796 15192.5 secs ago sensor:m_gps_mag_var(rad)=0.370009801422798 127.739 secs ago sensor:m_iridium_attempt_num(nodim)=1 122.419 secs ago sensor:m_iridium_call_num(nodim)=2545 67.03 secs ago sensor:m_iridium_dialed_num(nodim)=4634 93.974 secs ago sensor:m_leakdetect_voltage(volts)=2.49832112332112 4.694 secs ago sensor:m_leakdetect_voltage_forward(volts)=2.49410866910867 4.708 secs ago sensor:m_tot_num_inflections(nodim)=15572 398.423 secs ago sensor:m_vacuum(inHg)=8.99978241758241 14.325 secs ago sensor:m_water_vx(m/s)=-0.262257373397094 200.646 secs ago sensor:m_water_vy(m/s)=-0.161155863059387 200.678 secs ago sensor:sci_m_disk_free(Mbytes)=1987.28125 285.808 secs ago sensor:u_alt_min_depth(m)=2 1e+308 secs ago sensor:u_min_water_depth(m)=0 1e+308 secs ago sensor:u_use_current_correction(nodim)=0 1e+308 secs ago sensor:x_last_wpt_lat(lat)=-2330.0102 1e+308 secs ago sensor:x_last_wpt_lon(lon)=-4507.1071 1e+308 secs ago devices:(t/m/s) errs: 2/ 0/ 0 warn: 7/ 0/ 0 odd: 157/ 39/ 5 ABORT HISTORY: total since reset: 4 ABORT HISTORY: last abort cause: MS_ABORT_LEAK ABORT HISTORY: last abort details: There is a leak in the aft compartment. ABORT HISTORY: last abort time: 2014-11-19T10:12:54 ABORT HISTORY: last abort segment: ru29-2014-321-0-4 (0185.0004) ABORT HISTORY: last abort mission: 1K_N2.MI Hit Control-R to RESUME the mission, i.e. dive! Hit Control-C to END the mission, i.e. GliderDos Hit Control-E to extend surface time by 5 minutes. Hit Control-W to get device warning reports. Hit Control-F to re-read yo, goto_l, surface, sample, drift_ mafiles. Hit H <0:1> to Hangup and call back in minutes at 0-primary 1-alternate number. Hit S [-f={rf}|{irid] [-num=] [-t=] [filespec ...] to send log files Hit ! to execute Hit Control-T to consci to science computer when comms ready: ... communications ready for consci. Water Velocity Calculations waiting for final gps fix(ideally -86 secs) Waypoint: (-2440.0000,-4420.0000) Range: 43457m, Bearing: 66deg, Age: 4:21h:m Time until diving is: 465 secs Glider ru29 at surface. Because:no comms for a while [behavior surface_2 start_when = 12.0] MissionName:1K_N2.MI MissionNum:ru29-2014-322-1-10 (0187.0010) Vehicle Name: ru29 Curr Time: Thu Nov 20 05:27:39 2014 MT: 57018 DR Location: -2456.730 N -4438.154 E measured 167.86 secs ago GPS TooFar: -2453.952 N -4440.733 E measured 1e+308 secs ago GPS Invalid : -2456.421 N -4438.389 E measured 273.824 secs ago GPS Location: -2456.730 N -4438.154 E measured 170.244 secs ago sensor:c_thruster_surface_depth(m)=0 15227.7 secs ago sensor:c_thruster_surface_secs(s)=0 15227.7 secs ago sensor:c_wpt_lat(lat)=-2440 15738.1 secs ago sensor:c_wpt_lon(lon)=-4420 15738.1 secs ago sensor:m_battery(volts)=11.4075999092765 56.841 secs ago sensor:m_coulomb_amphr(amp-hrs)=19.4215621948242 4.416 secs ago sensor:m_coulomb_amphr_total(amp-hrs)=21.1035621949006 4.43 secs ago sensor:m_depth(m)=0.041478449970051 4.344 secs ago sensor:m_final_water_vx(m/s)=-0.179513337678253 15235.4 secs ago sensor:m_final_water_vy(m/s)=-0.139140604650796 15235.5 secs ago sensor:m_gps_mag_var(rad)=0.370009801422798 170.734 secs ago sensor:m_iridium_attempt_num(nodim)=1 165.415 secs ago sensor:m_iridium_call_num(nodim)=2545 110.025 secs ago sensor:m_iridium_dialed_num(nodim)=4634 136.97 secs ago sensor:m_leakdetect_voltage(volts)=2.49832112332112 47.69 secs ago sensor:m_leakdetect_voltage_forward(volts)=2.49410866910867 47.705 secs ago sensor:m_tot_num_inflections(nodim)=15572 441.419 secs ago sensor:m_vacuum(inHg)=8.99978241758241 57.321 secs ago sensor:m_water_vx(m/s)=-0.262257373397094 243.641 secs ago sensor:m_water_vy(m/s)=-0.161155863059387 243.674 secs ago sensor:sci_m_disk_free(Mbytes)=1987.28125 328.804 secs ago sensor:u_alt_min_depth(m)=2 1e+308 secs ago sensor:u_min_water_depth(m)=0 1e+308 secs ago sensor:u_use_current_correction(nodim)=0 1e+308 secs ago sensor:x_last_wpt_lat(lat)=-2330.0102 1e+308 secs ago sensor:x_last_wpt_lon(lon)=-4507.1071 1e+308 secs ago devices:(t/m/s) errs: 2/ 0/ 0 warn: 7/ 0/ 0 odd: 157/ 39/ 5 ABORT HISTORY: total since reset: 4 ABORT HISTORY: last abort cause: MS_ABORT_LEAK ABORT HISTORY: last abort details: There is a leak in the aft compartment. ABORT HISTORY: last abort time: 2014-11-19T10:12:54 ABORT HISTORY: last abort segment: ru29-2014-321-0-4 (0185.0004) ABORT HISTORY: last abort mission: 1K_N2.MI Hit Control-R to RESUME the mission, i.e. dive! Hit Control-C to END the mission, i.e. GliderDos Hit Control-E to extend surface time by 5 minutes. Hit Control-W to get device warning reports. Hit Control-F to re-read yo, goto_l, surface, sample, drift_ mafiles. Hit H <0:1> to Hangup and call back in minutes at 0-primary 1-alternate number. Hit S [-f={rf}|{irid] [-num=] [-t=] [filespec ...] to send log files Hit ! to execute Hit Control-T to consci to science computer when comms ready: ... communications ready for consci. Water Velocity Calculations waiting for final gps fix(ideally -129 secs) Waypoint: (-2440.0000,-4420.0000) Range: 43457m, Bearing: 66deg, Age: 4:22h:m Time until diving is: 422 secs Glider ru29 at surface. Because:no comms for a while [behavior surface_2 start_when = 12.0] MissionName:1K_N2.MI MissionNum:ru29-2014-322-1-10 (0187.0010) Vehicle Name: ru29 Curr Time: Thu Nov 20 05:28:23 2014 MT: 57062 DR Location: -2456.730 N -4438.154 E measured 212.048 secs ago GPS TooFar: -2453.952 N -4440.733 E measured 1e+308 secs ago GPS Invalid : -2456.421 N -4438.389 E measured 318.012 secs ago GPS Location: -2456.730 N -4438.154 E measured 214.432 secs ago sensor:c_thruster_surface_depth(m)=0 15271.9 secs ago sensor:c_thruster_surface_secs(s)=0 15271.9 secs ago sensor:c_wpt_lat(lat)=-2440 15782.2 secs ago sensor:c_wpt_lon(lon)=-4420 15782.3 secs ago sensor:m_battery(volts)=11.3893717864807 37.581 secs ago sensor:m_coulomb_amphr(amp-hrs)=19.4263114929199 4.373 secs ago sensor:m_coulomb_amphr_total(amp-hrs)=21.1083114929963 4.384 secs ago sensor:m_depth(m)=0.0138261499900002 4.301 secs ago sensor:m_final_water_vx(m/s)=-0.179513337678253 15279.6 secs ago sensor:m_final_water_vy(m/s)=-0.139140604650796 15279.6 secs ago sensor:m_gps_mag_var(rad)=0.370009801422798 214.892 secs ago sensor:m_iridium_attempt_num(nodim)=1 209.571 secs ago sensor:m_iridium_call_num(nodim)=2545 154.179 secs ago sensor:m_iridium_dialed_num(nodim)=4634 181.122 secs ago sensor:m_leakdetect_voltage(volts)=2.49496336996337 28.255 secs ago sensor:m_leakdetect_voltage_forward(volts)=2.49068986568986 28.267 secs ago sensor:m_tot_num_inflections(nodim)=15572 485.563 secs ago sensor:m_vacuum(inHg)=9.02953186813186 38.035 secs ago sensor:m_water_vx(m/s)=-0.262257373397094 287.781 secs ago sensor:m_water_vy(m/s)=-0.161155863059387 287.812 secs ago sensor:sci_m_disk_free(Mbytes)=1987.28125 372.939 secs ago sensor:u_alt_min_depth(m)=2 1e+308 secs ago sensor:u_min_water_depth(m)=0 1e+308 secs ago sensor:u_use_current_correction(nodim)=0 1e+308 secs ago sensor:x_last_wpt_lat(lat)=-2330.0102 1e+308 secs ago sensor:x_last_wpt_lon(lon)=-4507.1071 1e+308 secs ago devices:(t/m/s) errs: 2/ 0/ 0 warn: 7/ 0/ 0 odd: 157/ 39/ 5 ABORT HISTORY: total since reset: 4 ABORT HISTORY: last abort cause: MS_ABORT_LEAK ABORT HISTORY: last abort details: There is a leak in the aft compartment. ABORT HISTORY: last abort time: 2014-11-19T10:12:54 ABORT HISTORY: last abort segment: ru29-2014-321-0-4 (0185.0004) ABORT HISTORY: last abort mission: 1K_N2.MI Hit Control-R to RESUME the mission, i.e. dive! Hit Control-C to END the mission, i.e. GliderDos Hit Control-E to extend surface time by 5 minutes. Hit Control-W to get device warning reports. Hit Control-F to re-read yo, goto_l, surface, sample, drift_ mafiles. Hit H <0:1> to Hangup and call back in minutes at 0-primary 1-alternate number. Hit S [-f={rf}|{irid] [-num=] [-t=] [filespec ...] to send log files Hit ! to execute Hit Control-T to consci to science computer when comms ready: ... communications ready for consci. Water Velocity Calculations waiting for final gps fix(ideally -173 secs) Waypoint: (-2440.0000,-4420.0000) Range: 43457m, Bearing: 66deg, Age: 4:23h:m Time until diving is: 378 secs Glider ru29 at surface. Because:no comms for a while [behavior surface_2 start_when = 12.0] MissionName:1K_N2.MI MissionNum:ru29-2014-322-1-10 (0187.0010) Vehicle Name: ru29 Curr Time: Thu Nov 20 05:29:06 2014 MT: 57105 DR Location: -2456.730 N -4438.154 E measured 254.908 secs ago GPS TooFar: -2453.952 N -4440.733 E measured 1e+308 secs ago GPS Invalid : -2456.421 N -4438.389 E measured 360.871 secs ago GPS Location: -2456.730 N -4438.154 E measured 257.29 secs ago sensor:c_thruster_surface_depth(m)=0 15314.7 secs ago sensor:c_thruster_surface_secs(s)=0 15314.8 secs ago sensor:c_wpt_lat(lat)=-2440 15825.1 secs ago sensor:c_wpt_lon(lon)=-4420 15825.1 secs ago sensor:m_battery(volts)=11.385365987564 18.747 secs ago sensor:m_coulomb_amphr(amp-hrs)=19.429874420166 4.394 secs ago sensor:m_coulomb_amphr_total(amp-hrs)=21.1118744202424 4.405 secs ago sensor:m_depth(m)=0.262696849810469 4.321 secs ago sensor:m_final_water_vx(m/s)=-0.179513337678253 15322.5 secs ago sensor:m_final_water_vy(m/s)=-0.139140604650796 15322.5 secs ago sensor:m_gps_mag_var(rad)=0.370009801422798 257.755 secs ago sensor:m_iridium_attempt_num(nodim)=1 252.434 secs ago sensor:m_iridium_call_num(nodim)=2545 197.043 secs ago sensor:m_iridium_dialed_num(nodim)=4634 223.986 secs ago sensor:m_leakdetect_voltage(volts)=2.49945054945055 9.445 secs ago sensor:m_leakdetect_voltage_forward(volts)=2.49490231990232 9.457 secs ago sensor:m_tot_num_inflections(nodim)=15572 528.427 secs ago sensor:m_vacuum(inHg)=9.06713186813186 19.201 secs ago sensor:m_water_vx(m/s)=-0.262257373397094 330.646 secs ago sensor:m_water_vy(m/s)=-0.161155863059387 330.677 secs ago sensor:sci_m_disk_free(Mbytes)=1987.28125 415.804 secs ago sensor:u_alt_min_depth(m)=2 1e+308 secs ago sensor:u_min_water_depth(m)=0 1e+308 secs ago sensor:u_use_current_correction(nodim)=0 1e+308 secs ago sensor:x_last_wpt_lat(lat)=-2330.0102 1e+308 secs ago sensor:x_last_wpt_lon(lon)=-4507.1071 1e+308 secs ago devices:(t/m/s) errs: 2/ 0/ 0 warn: 7/ 0/ 0 odd: 157/ 39/ 5 ABORT HISTORY: total since reset: 4 ABORT HISTORY: last abort cause: MS_ABORT_LEAK ABORT HISTORY: last abort details: There is a leak in the aft compartment. ABORT HISTORY: last abort time: 2014-11-19T10:12:54 ABORT HISTORY: last abort segment: ru29-2014-321-0-4 (0185.0004) ABORT HISTORY: last abort mission: 1K_N2.MI Hit Control-R to RESUME the mission, i.e. dive! Hit Control-C to END the mission, i.e. GliderDos Hit Control-E to extend surface time by 5 minutes. Hit Control-W to get device warning reports. Hit Control-F to re-read yo, goto_l, surface, sample, drift_ mafiles. Hit H <0:1> to Hangup and call back in minutes at 0-primary 1-alternate number. Hit S [-f={rf}|{irid] [-num=] [-t=] [filespec ...] to send log files Hit ! to execute Hit Control-T to consci to science computer when comms ready: ... communications ready for consci. Water Velocity Calculations waiting for final gps fix(ideally -216 secs) Waypoint: (-2440.0000,-4420.0000) Range: 43457m, Bearing: 66deg, Age: 4:23h:m Time until diving is: 335 secs Glider ru29 at surface. Because:no comms for a while [behavior surface_2 start_when = 12.0] MissionName:1K_N2.MI MissionNum:ru29-2014-322-1-10 (0187.0010) Vehicle Name: ru29 Curr Time: Thu Nov 20 05:29:50 2014 MT: 57148 DR Location: -2456.730 N -4438.154 E measured 298.308 secs ago GPS TooFar: -2453.952 N -4440.733 E measured 1e+308 secs ago GPS Invalid : -2456.421 N -4438.389 E measured 404.27 secs ago GPS Location: -2456.730 N -4438.154 E measured 300.69 secs ago sensor:c_thruster_surface_depth(m)=0 15358.1 secs ago sensor:c_thruster_surface_secs(s)=0 15358.2 secs ago sensor:c_wpt_lat(lat)=-2440 15868.5 secs ago sensor:c_wpt_lon(lon)=-4420 15868.5 secs ago sensor:m_battery(volts)=11.385365987564 62.143 secs ago sensor:m_coulomb_amphr(amp-hrs)=19.4334373474121 4.413 secs ago sensor:m_coulomb_amphr_total(amp-hrs)=21.1154373474885 4.427 secs ago sensor:m_depth(m)=0.0691307499501017 4.343 secs ago sensor:m_final_water_vx(m/s)=-0.179513337678253 15365.8 secs ago sens ****** Glider ru29 at surface. Because:no comms for a while [behavior surface_2 start_when = 12.0] MissionName:1K_N2.MI MissionNum:ru29-2014-322-1-10 (0187.0010) Vehicle Name: ru29 Curr Time: Thu Nov 20 05:34:44 2014 MT: 57442 DR Location: -2456.730 N -4438.154 E measured 592.396 secs ago GPS TooFar: -2453.952 N -4440.733 E measured 1e+308 secs ago GPS Invalid : -2456.421 N -4438.389 E measured 698.362 secs ago GPS Location: -2456.730 N -4438.154 E measured 594.781 secs ago sensor:c_thruster_surface_depth(m)=0 15652.2 secs ago sensor:c_thruster_surface_secs(s)=0 15652.3 secs ago sensor:c_wpt_lat(lat)=-2440 16162.6 secs ago sensor:c_wpt_lon(lon)=-4420 16162.6 secs ago sensor:m_battery(volts)=11.3711175698111 38.195 secs ago sensor:m_coulomb_amphr(amp-hrs)=19.4595623016357 4.403 secs ago sensor:m_coulomb_amphr_total(amp-hrs)=21.1415623017121 4.415 secs ago sensor:m_depth(m)=0.0138261499900002 4.341 secs ago sensor:m_final_water_vx(m/s)=-0.179513337678253 15660 secs ago sensor:m_final_water_vy(m/s)=-0.139140604650796 15660 secs ago sensor:m_gps_mag_var(rad)=0.370009801422798 595.27 secs ago sensor:m_iridium_attempt_num(nodim)=1 589.951 secs ago sensor:m_iridium_call_num(nodim)=2545 534.561 secs ago sensor:m_iridium_dialed_num(nodim)=4634 561.506 secs ago sensor:m_leakdetect_voltage(volts)=2.49859584859585 33.648 secs ago sensor:m_leakdetect_voltage_forward(volts)=2.49377289377289 33.664 secs ago sensor:m_tot_num_inflections(nodim)=15572 865.955 secs ago sensor:m_vacuum(inHg)=9.05060439560439 38.675 secs ago sensor:m_water_vx(m/s)=-0.262257373397094 668.177 secs ago sensor:m_water_vy(m/s)=-0.161155863059387 668.209 secs ago sensor:sci_m_disk_free(Mbytes)=1987.28125 753.34 secs ago sensor:u_alt_min_depth(m)=2 1e+308 secs ago sensor:u_min_water_depth(m)=0 1e+308 secs ago sensor:u_use_current_correction(nodim)=0 1e+308 secs ago sensor:x_last_wpt_lat(lat)=-2330.0102 1e+308 secs ago sensor:x_last_wpt_lon(lon)=-4507.1071 1e+308 secs ago devices:(t/m/s) errs: 2/ 0/ 0 warn: 7/ 0/ 0 odd: 157/ 39/ 5 ABORT HISTORY: total since reset: 4 ABORT HISTORY: last abort cause: MS_ABORT_LEAK ABORT HISTORY: last abort details: There is a leak in the aft compartment. ABORT HISTORY: last abort time: 2014-11-19T10:12:54 ABORT HISTORY: last abort segment: ru29-2014-321-0-4 (0185.0004) ABORT HISTORY: last abort mission: 1K_N2.MI Hit Control-R to RESUME the mission, i.e. dive! Hit Control-C to END the mission, i.e. GliderDos Hit Control-E to extend surface time by 5 minutes. Hit Control-W to get device warning reports. Hit Control-F to re-read yo, goto_l, surface, sample, drift_ mafiles. Hit H <0:1> to Hangup and call back in minutes at 0-primary 1-alternate number. Hit S [-f={rf}|{irid] [-num=] [-t=] [filespec ...] to send log files Hit ! to execute Hit Control-T to consci to science computer when comms ready: ... communications ready for consci. Water Velocity Calculations waiting for final gps fix(ideally -554 secs) Waypoint: (-2440.0000,-4420.0000) Range: 43457m, Bearing: 66deg, Age: 4:29h:m Time until diving is: -2 secs Megabytes used on CF file system = 64.593750 Megabytes available on CF file system = 1933.375000 57448 40 01870010.mlg LOG FILE CLOSED Doing system wide housekeeping....... report_heap_size(): M_FREE_HEAP=245.0K, M_SPARE_HEAP=226.0K Running algorithm to free disk space if required Not necessary to delete any files at this time Writing longterm state disk file: c:/state/longterm.sta f_coulomb_battery_capacity(amp-hrs) 1018.000000 f_fin_safety_max(rad) 0.320000 f_ocean_pressure_min(volts) 0.099557 m_avg_climb_rate(m/s) -0.247572 m_avg_speed(m/s) 0.306279 m_avg_upward_inflection_time(sec) 46.557953 m_battery(volts) 11.371118 m_coulomb_amphr_total(amp-hrs) 21.142751 m_iridium_call_num(nodim) 2545.000000 m_iridium_dialed_num(nodim) 4634.000000 m_lat(lat) -2456.730200 m_lon(lon) -4438.154100 m_tot_ballast_pumped_energy(kjoules) 0.000000 m_tot_horz_dist(km) 12265.600730 m_tot_num_inflections(nodim) 15572.000000 s_water_depth_avg(m) 200.000000 s_water_depth_delta(m) 0.000000 s_water_depth_wavelength(m) 100.000000 u_max_time_in_gliderdos(sec) 900.000000 x_de_avg_oil_vol_ierr_on_ascent(cc) 0.000000 x_de_avg_oil_vol_ierr_on_descent(cc) 0.000000 x_hover_ballast_deep(cc) 0.000000 x_hover_ballast_shallow(cc) 0.000000 x_hover_depth_deep(m) 0.000000 x_hover_depth_shallow(m) 0.000000 x_last_wpt_lat(lat) -2330.010200 x_last_wpt_lon(lon) -4507.107100 The instantaneous lag time between the system and gps clock is -4.0 seconds. The average lag time between the system and gps clock is -3.6 seconds. Housekeeping is done 57508 45 01870011.mlg LOG FILE OPENED Megabytes used on CF file system = 64.656250 Megabytes available on CF file system = 1933.312500 57510 init_gps_input() 57510 behavior surface_2: SUBSTATE 7 ->10 : Waiting for final gps fix 57511 behavior surface_2: TIMED OUT WAITING FOR A CHARACTER surface_2: Waiting for final GPS fix. 57513 disabling Iridium console...