60672 Iridium console active and ready... Vehicle Name: ru29 Curr Time: Wed Nov 19 11:28:11 2014 MT: 60672 DR Location: -2456.591 N -4439.389 E measured 128.592 secs ago GPS TooFar: -2453.952 N -4440.733 E measured 14402.9 secs ago GPS Invalid : -2454.005 N -4440.750 E measured 2918.72 secs ago GPS Location: -2456.595 N -4439.397 E measured 548.475 secs ago sensor:c_thruster_surface_depth(m)=0 14446.8 secs ago sensor:c_thruster_surface_secs(s)=0 14446.8 secs ago sensor:c_wpt_lat(lat)=-2530 37974 secs ago sensor:c_wpt_lon(lon)=-4410 37974.1 secs ago sensor:m_battery(volts)=11.2594737174165 4.28 secs ago sensor:m_coulomb_amphr(amp-hrs)=15.6844997406006 4.455 secs ago sensor:m_coulomb_amphr_total(amp-hrs)=17.366499740677 4.469 secs ago sensor:m_depth(m)=0 4.351 secs ago sensor:m_final_water_vx(m/s)=-0.0515394562790794 14454.6 secs ago sensor:m_final_water_vy(m/s)=-0.119091093391244 14454.7 secs ago sensor:m_gps_mag_var(rad)=0.370009801422798 548.971 secs ago sensor:m_iridium_attempt_num(nodim)=2 42.129 secs ago sensor:m_iridium_call_num(nodim)=2532 0.649 secs ago sensor:m_iridium_dialed_num(nodim)=4616 12.928 secs ago sensor:m_leakdetect_voltage(volts)=2.49954212454212 41.985 secs ago sensor:m_leakdetect_voltage_forward(volts)=2.49481074481074 42 secs ago sensor:m_tot_num_inflections(nodim)=15508 5961.22 secs ago sensor:m_vacuum(inHg)=9.06258681318681 4.768 secs ago sensor:m_water_vx(m/s)=-0.0515394562790794 14455 secs ago sensor:m_water_vy(m/s)=-0.119091093391244 14455 secs ago sensor:sci_m_disk_free(Mbytes)=1989.53125 14541 secs ago sensor:u_alt_min_depth(m)=2 1e+308 secs ago sensor:u_min_water_depth(m)=0 1e+308 secs ago sensor:u_use_current_correction(nodim)=0 1e+308 secs ago sensor:x_last_wpt_lat(lat)=-2330.0102 1e+308 secs ago sensor:x_last_wpt_lon(lon)=-4507.1071 1e+308 secs ago ABORT HISTORY: total since reset: 4 ABORT HISTORY: last abort cause: MS_ABORT_LEAK ABORT HISTORY: last abort details: There is a leak in the aft compartment. ABORT HISTORY: last abort time: 2014-11-19T10:12:54 ABORT HISTORY: last abort segment: ru29-2014-321-0-4 (0185.0004) ABORT HISTORY: last abort mission: 1K_N2.MI 60673 No login script found for processing. GliderDos A 24 >get f_leakdetect_threshold = 0.750000 volts GliderDos A 24 >zr 60709 11 save_and_change_sensors().... Changed u_use_ctd_depth_for_flying from 0 to 0 Changed c_science_on from 1 to 0 60709 save_and_change_sensors().... Changed c_science_printout from 0 to 0 Waiting for motors idle START **B01000800275775 � 60759 restore_sensors().... Restored u_use_ctd_depth_for_flying from 0 to 0 Restored c_science_on from 0 to 1 60759 restore_sensors().... 60759 restore_sensors().... Restored c_science_printout from 0 to 0 Done! GliderDos A 24 > 60766 12 SCI:PROGLET house_elf begin() called 60766 SCI: house_elf: Version 1.2 60766 SCI:PROGLET ctd41cp begin() called 60766 SCI: ctd41cp: Version 0.2 60767 SCI: ctd41cp: Will be sending the following data to glider: 60767 SCI: sci_water_cond(s/m) 60767 SCI: sci_water_temp(degc) 60767 SCI: sci_water_pressure(bar) 60767 SCI: sci_ctd41cp_timestamp(timestamp) 60769 13 SCI:PROGLET house_elf start() called 60769 SCI: house_elf_run(): 0 error(s) in a row. (5 is fatal) 60769 SCI: house_elf_run(): 0 error(s) since house_elf_begin(). (50 is fatal) GliderDos A 24 >zr 60838 31 save_and_change_sensors().... Changed u_use_ctd_depth_for_flying from 0 to 0 Changed c_science_on from 1 to 0 60838 save_and_change_sensors().... Changed c_science_printout from 0 to 0 Waiting for motors idle START **B01000800275775 � 60870 restore_sensors().... Restored u_use_ctd_depth_for_flying from 0 to 0 Restored c_science_on from 0 to 1 60870 restore_sensors().... 60870 restore_sensors().... Restored c_science_printout from 0 to 0 Done! GliderDos A 24 >sbd load sbdlist.dat ---Writing new *.sbd config file to disk GliderDos A 24 > 60883 34 SCI:PROGLET house_elf start() called 60883 SCI: house_elf_run(): 0 error(s) in a row. (5 is fatal) 60884 SCI: house_elf_run(): 0 error(s) since house_elf_begin(). (50 is fatal) sequence 1k_n2.mi(5) Sequencing missions load_mission(): Opening Mission file: 1K_N2.MI for execution 5 times Setting SENSOR c_science_all_on_enabled(bool) = 0.000000 Setting SENSOR c_science_send_all(bool) = 0.000000 Setting SENSOR u_dbd_sensor_list_xmit_control(enum) = 3.000000 Setting SENSOR u_sci_dbd_sensor_list_xmit_control(enum) = 2.000000 Exiting all devices ... 60893 37 disabling Iridium cons