NO CARRIER RING CONNECT 4800/ARQ/V32/LAPM 1225 Iridium console active and ready... Vehicle Name: silbo Curr Time: Sat Aug 3 16:30:24 2013 MT: 1222 DR Location: 1330.664 N -4714.147 E measured 1e+308 secs ago GPS TooFar: 69696969.000 N 69696969.000 E measured 1e+308 secs ago GPS Invalid : 69696969.000 N 69696969.000 E measured 1e+308 secs ago GPS Location: 69696969.000 N 69696969.000 E measured 1e+308 secs ago sensor:c_autoballast_state(enum)=0 1e+308 secs ago sensor:c_climb_bpump(X)=1000 1e+308 secs ago sensor:c_dive_bpump(X)=-1000 1e+308 secs ago sensor:c_wpt_lat(lat)=0 1e+308 secs ago sensor:c_wpt_lon(lon)=0 1e+308 secs ago sensor:m_battery(volts)=11.0134486044168 1183.37 secs ago sensor:m_coulomb_amphr(amp-hrs)=0.14962500333786 15.78 secs ago sensor:m_coulomb_amphr_total(amp-hrs)=654.804124503376 15.802 secs ago sensor:m_final_water_vx(m/s)=0 1e+308 secs ago sensor:m_final_water_vy(m/s)=0 1e+308 secs ago sensor:m_iridium_signal_strength(nodim)=5 31.227 secs ago sensor:m_leakdetect_voltage(volts)=2.49395604395604 1183.62 secs ago sensor:m_leakdetect_voltage_forward(volts)=2.48873626373626 1183.65 secs ago sensor:m_tot_num_inflections(nodim)=7260 1e+308 secs ago sensor:m_vacuum(inHg)=8.33039902319902 1183.93 secs ago sensor:m_water_vx(m/s)=0 1e+308 secs ago sensor:m_water_vy(m/s)=0 1e+308 secs ago sensor:u_use_current_correction(nodim)=1 1e+308 secs ago sensor:x_last_wpt_lat(lat)=1008.2667 1e+308 secs ago sensor:x_last_wpt_lon(lon)=-3537.1998 1e+308 secs ago ABORT HISTORY: total since reset: 1 ABORT HISTORY: last abort cause: MS_ABORT_LOW_REL_CHARGE ABORT HISTORY: last abort details: ABORT HISTORY: last abort time: 2013-08-03T16:13:41 ABORT HISTORY: last abort segment: silbo-2013-214-0-0 (0078.0000) ABORT HISTORY: last abort mission: initial.mi 1226 No login script found for processing. 1226 DRIVER_ODDITY:iridium:1929:xxx_ctrl() ran too long 1227 sensor: m_depth = 17.229437785528 m 1237 83 Attempting to put only critical devices back into service 1237 behavior ?_-1: Vehicle Name: silbo 1238 behavior ?_-1: abort_the_mission(): (32)MS_ABORT_LOW_REL_CHARGE 1238 behavior ?_-1: secs since abort started: 1085 try num: 72 1238 behavior ?_-1: depths ini: 17 working: 1050 at risk: 1196 crush: 1200 1238 behavior ?_-1: expected time/tries to surface: 564 37 1238 behavior ?_-1: max time/tries to go up: 300 20 1238 behavior ?_-1: too long: 1, not going up: 1, depth sensor busted:0 1238 behavior ?_-1: abort burn time/tries min: 600 40 1238 behavior ?_-1: abort burn time/tries max: 14400 960 1238 behavior ?_-1: ABOVE WORKING DEPTH 1238 behavior ?_-1: drop_the_weight = 0 1238 Not recommended, but if in infinite loop, hit Control-C 1242 sensor: m_depth = 20.5253732379281 m 1252 84 Attempting to put everything back into service 1252 behavior ?_-1: Vehicle Name: silbo 1253 behavior ?_-1: abort_the_mission(): (32)MS_ABORT_LOW_REL_CHARGE 1253 behavior ?_-1: secs since abort started: 1100 try num: 73 1253 behavior ?_-1: depths ini: 17 working: 1050 at risk: 1196 crush: 1200 1253 behavior ?_-1: expected time/tries to surface: 564 37 1253 behavior ?_-1: max time/tries to go up: 300 20 1253 behavior ?_-1: too long: 1, not going up: 1, depth sensor busted:0 1253 behavior ?_-1: abort burn time/tries min: 600 40 1253 behavior ?_-1: abort burn time/tries max: 14400 960 1253 behavior ?_-1: ABOVE WORKING DEPTH 1253 behavior ?_-1: drop_the_weight = 0 1253 Not recommended, but if in infinite loop, hit Control-C 1255 sensor: m_depth = 21.8212111081025 m 1267 85 Attempting to put only critical devices back into service 1267 behavior ?_-1: Vehicle Name: silbo 1268 behavior ?_-1: abort_the_mission(): (32)MS_ABORT_LOW_REL_CHARGE 1268 behavior ?_-1: secs since abort started: 1115 try num: 74 1268 behavior ?_-1: depths ini: 17 working: 1050 at risk: 1196 crush: 1200 1268