Fleet Configurations
Deployments
Gliders
Projects
Payload Bays
Instruments
Users
API
Log In
Deployment ru25d-20171222T1251
Pilot Notes
Glider got stuck on bottom and shot its weight. Bottom angle from altimeter data was 30 degrees. We were inflecting 30 m off bottom. Of course the sea mount can't rise forever but eventually 30 and 26 have colliding paths. New protocol needed for Antarctic gliders, maybe steeper climb angles. ru25 drifting since weight likely gone and fin is no longer working. Not sure if fin not working is related to being stuck or not or if digifin leak got bad enough. Fin stuck at ~0 and wont move without the following: 49653 51 DRIVER_WARNING:digifin:-1:digifin_v2_ctrl() Digifin movement warning. Digifin busy too long!!!
Category
Informational
Alert
Action Needed
Action Taken
Operations
Update
Credentials Required
Username
Password